ASN Wikibase Occurrence # 170334
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Date: | Monday 22 September 2014 |
Time: | 10:18 |
Type: | Cessna U206C |
Owner/operator: | 70 North |
Registration: | N206J |
MSN: | U206-0965 |
Year of manufacture: | 1967 |
Total airframe hrs: | 6987 hours |
Engine model: | Continental. IO-520-F48B |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 14 miles east-northeast of Deadhorse, Alaska -
United States of America
|
Phase: | Initial climb |
Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
Departure airport: | Deadhorse, AK (AK78) |
Destination airport: | Deadhorse, AK (SCC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was conducting an on-demand air taxi commuter flight. The pilot reported that, during cruise flight, the engine began vibrating violently and lost power and that the throttle and propeller controls were unresponsive. The cockpit subsequently filled with smoke. The pilot conducted a forced landing to the nearest and driest tundra patch, during which the airplane nosed over.
Examination of the engine revealed a large hole on the top left side of the crankcase near the No. 2 cylinder. The No. 2 connecting rod had separated from the crankshaft connecting rod journal. The No. 2 main bearing support mating surfaces exhibited fretting damage. The No. 2 main bearing had shed material from its forward side and had shifted. Measurements of the breakaway torque on the cylinder through bolts indicated that the torque on the Nos. 2 and 3 cylinder through bolts was below the engine manufacturer’s specification. It is likely that the insufficient torque on the Nos. 2 and 3 cylinder through bolts resulted in the fretting damage and the No. 2 main bearing shifting and interrupted the oil flow to the No. 2 connecting rod bearing. The interruption of oil flow resulted in the bearing becoming starved of oil and overheating and the subsequent separation of the connecting rod from the crankshaft.
A review of maintenance records revealed that the No. 1 cylinder was replaced about 403 flight hours before the accident, which would have required the removal and installation of hardware on the Nos. 1, 2, and 3 cylinder through bolts. It is likely that insufficient torque was applied to the through bolts during the replacement of the No. 1 cylinder.
Probable Cause: The application of insufficient torque to the engine cylinder through bolts during the replacement of the No. 1 cylinder, which resulted in the displacement of the No. 2 bearing, oil starvation, and a catastrophic engine failure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC14LA085 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2014 11:00 |
Aerossurance |
Added |
07-Oct-2014 22:00 |
Geno |
Updated [Departure airport, Destination airport, Source] |
24-Apr-2016 15:49 |
Aerossurance |
Updated [Time, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:12 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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