ASN Wikibase Occurrence # 170563
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Date: | Tuesday 21 October 2014 |
Time: | 17:45 |
Type: | Zenair CH 601 XL Zodiac |
Owner/operator: | Private |
Registration: | N601WR |
MSN: | 6-4958 |
Total airframe hrs: | 4 hours |
Engine model: | Wynn Corvair |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Baxter County Airport (KBPK), Mountain Home, AR -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Mountain Home, AR (BPK) |
Destination airport: | Mountain Home, AR (BPK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had recently built the airplane. The pilot operated the engine for about 4 hours, and the engine operated normally during the ground tests. During takeoff on the airplane’s first flight, he advanced the throttle slowly to 2,550 rpm, and the airplane lifted off the runway about 60 mph. About three-quarters down the runway and about 50 ft above ground level, the engine began to lose power. The pilot attempted to return to the runway by turning left. The pilot completed a 180-degree left turn, but the engine rpm had reduced to about 1,925 rpm, and the airplane was unable to maintain altitude. Data from the airplane’s engine monitoring device (EMD) indicated that the airplane reached a maximum airspeed of about 65 mph; the last airspeed reading before ground impact was 41 mph. The pilot attempted to land in a small clearing, but the airplane clipped a tree before landing. The airplane sustained substantial damage to the wings and fuselage during the ground impact.
Data from the EMD also indicated that the engine operated for about 12 minutes from engine start to ground impact. The data indicated that the engine oil pressure, engine oil temperature, and fuel pressure were normal throughout the flight but that the Nos. 2, 3, and 5 cylinder head temperatures exceeded 500 degrees F. A postaccident examination of the engine and carburetor revealed no evidence of mechanical malfunctions, heat distress, or failures that would have precluded the engine’s operation. The reason for the increased cylinder head temperature indications and the partial power loss could not be determined.
Probable Cause: The partial loss of engine power during takeoff for reasons that could not be determined because postaccident engine examinations revealed no anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA023 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=601WR Location
Revision history:
Date/time | Contributor | Updates |
22-Oct-2014 03:26 |
Geno |
Added |
22-Oct-2014 03:34 |
Geno |
Updated [Phase, Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:29 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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