ASN Wikibase Occurrence # 174250
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Date: | Tuesday 3 March 2015 |
Time: | 12:15 |
Type: | Fisher Classic |
Owner/operator: | Goudie Lawrence A |
Registration: | N417LG |
MSN: | C0145 |
Year of manufacture: | 2013 |
Total airframe hrs: | 47 hours |
Engine model: | Continental A-80-8 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | East of Redlands Municipal Airport (KREI), Redlands, CA -
United States of America
|
Phase: | Landing |
Nature: | Test |
Departure airport: | Redlands, CA (REI) |
Destination airport: | Redlands, CA (REI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the purpose of the flight was to determine how much unusable fuel was in the experimental amateur-built airplane’s fuel tanks. The airplane took off with a full header tank and only 1 gallon of fuel in each wing tank. After takeoff, the pilot climbed the airplane to about 3,500 ft, and, about 3 miles from the airport, he switched from the header tank to the right fuel tank. Shortly after, the engine suddenly stopped, and the propeller stopped turning. The pilot quickly switched back to the header tank. Since the airplane was not equipped with a starter, the pilot initiated a dive to attempt to get the propeller spinning but was unsuccessful; he could not restart the engine. The pilot leveled the airplane to attain its best glide speed and proceeded toward a road. He subsequently landed the airplane on a rocky riverbank short of the road. The pilot reported that there were no mechanical failures or malfunctions with the engine or airframe that would have precluded normal operation. The pilot further reported that he should have considered the possibility that the engine might stop and that he should have flown the airplane at a higher altitude and remained closer to the airport where he could have made a dead-stick landing if necessary.
Probable Cause: A loss of engine power due to fuel starvation. Contributing to the accident was the pilot's inadequate planning for the test flight, which resulted in insufficient altitude and no suitable place to land in the event of an emergency.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15LA123 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=417LG Location
Revision history:
Date/time | Contributor | Updates |
04-Mar-2015 03:18 |
Geno |
Added |
20-Mar-2015 23:23 |
Geno |
Updated [Time, Phase, Nature, Departure airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 12:45 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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