ASN Wikibase Occurrence # 17527
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Date: | Sunday 20 April 2008 |
Time: | 21:00 |
Type: | Cessna 172L |
Owner/operator: | Green Castle Aeor Club Ltd. |
Registration: | N9832G |
MSN: | 17259732 |
Year of manufacture: | 1971 |
Total airframe hrs: | 8815 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | about 2.5 miles north of Fairfax, Iowa -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Waterloo, IA (ALO) |
Destination airport: | Oxford, IA (IA24) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on a 3-leg round-robin flight under night visual meteorological (VMC) conditions. He did not refuel the airplane prior to departure. During the second leg of the flight, the pilot picked up two passengers and flew for about 30 minutes and deplaned them at the same airport. Then the pilot continued on the third flight leg. He was en route at 3,000 feet msl when the engine began to run rough and lost about 50 percent of its power. The pilot reported that the engine quit and he executed a forced landing to a field. The airplane nosed over in the soft soil. The Hobbs meter indicated that the accident flight was 2.9 hours in length. The pilot who flew the accident airplane previously that day reported that he did not top off the fuel prior to the 1.1-hour flight that he flew. He did not add fuel after the flight, which left about 22.3 gallons of useable fuel on board the airplane. The Pilot Operating Handbook (POH) indicated that the airplane used about 9.7 gallons of fuel during the 1.1 hour flight. According to the POH, the airplane used about 7.9 gallons per hour in cruise flight at 2,500 feet msl. An additional 1-gallon of fuel was consumed in the climb to 2,500 feet msl. The estimated fuel consumed during the accident flight was about 23.9 gallons.
Probable Cause: Fuel exhaustion as a result of the pilot's inadequate preflight inspection and inaccurate fuel calculations.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08LA108 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
22-Apr-2008 11:59 |
Fusko |
Added |
25-Apr-2008 11:08 |
Fusko |
Updated |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 10:43 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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