ASN Wikibase Occurrence # 176231
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Date: | Tuesday 19 May 2015 |
Time: | 18:30 |
Type: | Piper PA-22 |
Owner/operator: | Private |
Registration: | N118U |
MSN: | 22-3988 |
Year of manufacture: | 1956 |
Total airframe hrs: | 3586 hours |
Engine model: | Lycoming 0-320-A4A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near St Charles County Smartt Airport (KSET), St Charles, MO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | St. Charles, MO (SET) |
Destination airport: | St. Charles, MO (SET) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that, while approaching the airport to land, he turned on the boost pump, reduced the throttle, and applied carburetor heat. While on downwind, he reduced the engine power to idle and lowered the flaps. While on the base leg, he advanced the throttle; however, the engine stayed at idle power. He turned off the carburetor heat, adjusted the throttle, and cycled the boost pump but was unable to regain engine power and elected to perform a forced landing to a plowed field. The airplane contacted a ditch at the end of the field, crossed over a road, and came to rest in another field, resulting in substantial damage.
A postaccident examination of the airplane revealed that the fuel level in the right wing tank was "low" and the left wing fuel tank was about half full of fuel. A test run of the engine revealed no anomalies. The temperature and dew point conditions were conducive to the formation of serious carburetor icing at glide power; however, the pilot reported that he had applied carburetor heat during the descent and that it was on when the engine would not regain power.
Probable Cause: A loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA237 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=118U Location
Revision history:
Date/time | Contributor | Updates |
20-May-2015 04:13 |
Geno |
Added |
20-May-2015 07:15 |
Red Baron |
Updated [Aircraft type] |
20-May-2015 07:15 |
harro |
Updated [Aircraft type] |
20-May-2015 15:02 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 13:08 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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