ASN Wikibase Occurrence # 176805
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Date: | Wednesday 10 June 2015 |
Time: | 05:40 |
Type: | Piper PA-28R-200 Arrow II |
Owner/operator: | Private |
Registration: | N872CS |
MSN: | 28R-7635304 |
Year of manufacture: | 1976 |
Total airframe hrs: | 3831 hours |
Engine model: | Lycoming IO-360-C1C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Jonesboro Municipal Airport (KJBR), Jonesboro, AR -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Jonesboro, AR (JBR) |
Destination airport: | Stillwater, OK (SBR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was taking off for a personal flight. The pilot reported that, about 3 to 5 minutes after takeoff, the oil light illuminated and that, shortly thereafter, while the airplane was about 1,800 ft mean sea level, the oil pressure gauge indicated 0. About 20 to 30 seconds later, a total loss of engine power occurred. The pilot attempted to return to the departure airport but was unable to reach the runway due to insufficient altitude. The pilot subsequently conducted a forced landing in a parking lot, during which the airplane impacted a sign pole.
Examination of the airplane revealed that, during retraction, the nose landing gear (NLG) had contacted and broken the engine oil drain valve, which was the incorrect part number. The airplane manufacturer had previously issued a service letter, which noted that, when the wrong part number drain valve was installed, it was possible that during NLG retraction the valve may contact the NLG drag link, become actuated, and allow the oil to be drained out in flight. The accident flight was the first flight since the drain valve had been replaced the previous day during a 100-hour/annual inspection. Given the evidence, maintenance personnel did not install the correct part number drain valve during the inspection, which resulted in it contacting the NLG and breaking. The oil then drained from the broken valve, which resulted in oil exhaustion and the subsequent loss of engine power.
Probable Cause: Maintenance personnel's improper engine oil drain valve installation, which led to engine oil exhaustion and the subsequent loss of engine power after takeoff at an altitude too low for the pilot to execute a forced landing in a suitable area.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA270 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=872CS Location
Revision history:
Date/time | Contributor | Updates |
10-Jun-2015 15:38 |
Geno |
Added |
10-Jun-2015 16:19 |
Anon. |
Updated [Total fatalities] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 13:43 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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