Accident Mooney M20E Super 21 N5863Q,
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ASN Wikibase Occurrence # 182351
 
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Date:Monday 14 December 2015
Time:13:41
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20E Super 21
Owner/operator:Private
Registration: N5863Q
MSN: 796
Year of manufacture:1965
Total airframe hrs:4480 hours
Engine model:Lycoming IO-360 SER
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near Corona Municipal Airport (KAJO), Corona, CA -   United States of America
Phase: Take off
Nature:Private
Departure airport:Corona, CA (AJO)
Destination airport:Chino Airport, CA (CNO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot reported that the accident flight was the airplane’s first flight after being painted. After completing a preflight inspection, the pilot started the engine and observed a decrease in power. He leaned the mixture slightly, and the engine rpm returned to normal idle speed. The pilot reported that during the engine run-up, he noticed that the engine had a delayed response when he increased the throttle, but that the run-up otherwise revealed no anomalies. The pilot stated that the takeoff roll took longer than expected, and after lifting off near the end of the runway, the airplane climbed more slowly than normal. The pilot stated that during the initial climb, engine power had decreased to 2,000 rpm. As the airplane reached about 100 ft above ground level, the engine was producing about 1,800 rpm and could not maintain a climb. The pilot elected to continue straight ahead rather than return to the runway, and the airplane subsequently descended into trees. A postaccident examination revealed no anomalies with the airframe or engine that would have precluded normal operation. The reason for the partial loss of engine power was not determined.

Probable Cause: A partial loss of engine power during initial climb for reasons that could not be determined based on available information. Contributing to the accident was the pilot’s decision to conduct the takeoff with observed engine deficiencies.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR16LA039
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
15-Dec-2015 18:50 Geno Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
19-Aug-2017 14:56 ASN Update Bot Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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