Accident Ryan Navion B N5294K,
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ASN Wikibase Occurrence # 188973
 
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Date:Saturday 30 July 2016
Time:12:30
Type:Silhouette image of generic NAVI model; specific model in this crash may look slightly different    
Ryan Navion B
Owner/operator:Private
Registration: N5294K
MSN: NAV-4-2194B
Year of manufacture:1950
Total airframe hrs:3033 hours
Engine model:Continental IO-550-B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Manitowoc County Airport (KMTW), Manitowoc, WI -   United States of America
Phase: Take off
Nature:Private
Departure airport:Manitowoc, WI (MTW)
Destination airport:Manitowoc, WI (MTW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the private pilot, the engine run-up, taxi to the runway, and takeoff were normal. After establishing a positive climb rate, the pilot retracted the landing gear. Shortly after the gear retraction, the engine lost total power. The pilot quickly tried to restart the engine without success and then conducted a forced landing on the remaining runway. The airplane impacted the side of the runway and came to rest upright.
An examination of the engine revealed no anomalies. No fuel was found in the fuel lines from the firewall to the engine fuel system components. The fuel selector valve and gascolator were removed for further examination and testing. A vacuum test of the fuel selector valve revealed no anomalies. The gascolator exhibited fuel staining on the top of the casting. A vacuum test of the gascolator revealed that it leaked severely due to degraded rubber gaskets. It is likely that the leaks in the gascolator allowed air to enter the fuel system and resulted in the loss of engine power. The pilot stated that he typically needed to use the electric fuel boost pump in the low position to keep the engine running smoothly during the run-up and taxi until the engine reached normal operating temperature, which was contrary to the airplane checklist that was provided by the pilot. 

Probable Cause: A leak in the gascolator due to degraded rubber gaskets, which allowed air to enter the fuel system and resulted in fuel starvation and a total loss of engine power during takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN16LA296
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
https://flightaware.com/resources/registration/N5294K

Location

Revision history:

Date/timeContributorUpdates
01-Aug-2016 01:28 Geno Added
02-Aug-2016 17:06 Iceman 29 Updated [Registration, Cn, Source]
02-Aug-2016 17:06 harro Updated [Aircraft type, Operator]
19-Aug-2017 14:56 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative]

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