Hard landing Accident Cessna U206G Turbine Stationair N891LL,
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ASN Wikibase Occurrence # 189560
 
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Date:Thursday 25 August 2016
Time:10:05
Type:Silhouette image of generic C206 model; specific model in this crash may look slightly different    
Cessna U206G Turbine Stationair
Owner/operator:State Of Illinois
Registration: N891LL
MSN: U206-06937
Year of manufacture:1986
Total airframe hrs:6170 hours
Engine model:Allison 250-C20S
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Loves Corner N of Cave-In-Rock, IL -   United States of America
Phase: En route
Nature:Survey
Departure airport:Springfield, IL (SPI)
Destination airport:Springfield, IL (SPI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline transport pilot and camera operator were conducting an aerial mapping flight. While level at 3,500 ft above ground level, the turbo propeller-equipped airplane experienced a total loss of engine power. The pilot attempted to restart the engine three times without success. During the subsequent forced landing, the airplane struck a berm, which damaged both wings.
Examination of the engine revealed that fuel would not flow to the fuel nozzle until air pressure was bled upstream of the check valve assembly, located between the engine fuel control and the fuel nozzle. After the air pressure was bled and the fuel pump purged, normal fuel flow resumed, indicating that air had entered the fuel system. Because of the check valve assembly design, an in-flight engine restart was not possible after air entered the fuel line, and there was no procedure to clear air from the fuel line while in flight. Examination of the engine and fuel system could not establish a reason for air entering the fuel line.   

Probable Cause: A total loss of engine power due to air entering the fuel system for reasons that could not be determined based on available information. Contributing to the accident was the pilot’s inability to restart the engine due to the check valve assembly design.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN16LA335
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=891LL

Location

Revision history:

Date/timeContributorUpdates
25-Aug-2016 20:52 Geno Added
25-Aug-2016 21:21 Geno Updated [Aircraft type, Registration, Cn, Operator, Source]
16-Sep-2018 18:15 ASN Update Bot Updated [Time, Operator, Total occupants, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]
16-Sep-2018 18:53 harro Updated [Phase, Nature, Source, Narrative]

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