ASN Wikibase Occurrence # 190372
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Date: | Thursday 22 September 2016 |
Time: | 10:55 |
Type: | Scottish Aviation Bulldog 101 |
Owner/operator: | Private |
Registration: | N432BD |
MSN: | 163 |
Year of manufacture: | 1972 |
Total airframe hrs: | 5370 hours |
Engine model: | Lycoming IO-360-A1B6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Wichita, KS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Augusta Muni, KS (3AU) |
Destination airport: | Augusta Muni, KS (3AU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot reported that the engine "sputtered and went to idle" during cruise flight while returning to the departure airport after a local flight. His attempts to restore engine power were not successful. The pilot subsequently conducted a forced landing, during which the airplane impacted a fence and sustained substantial damage.
During postaccident examination, the fuel totalizer indicated that 7.3 gallons of fuel remained; however, only about 1.5 gallons of fuel was recovered from the airplane. After fuel was added to each tank, an engine run was conducted, and the engine ran smoothly at idle and about 1,000 rpm, and no anomalies were noted.
The pilot reported that the airplane fuel gauges were unreliable, so he used the fuel totalizer for fuel quantity information. However, the totalizer’s operating instructions stated that the instrument does not provide a measurement of the fuel in the tanks and that it “should never be used as the primary indicator of the fuel quantity.” The pilot should not have used the totalizer to determine the amount of fuel onboard the airplane and his reliance on the instrument without ensuring that sufficient fuel was on board for the flight led to fuel exhaustion and a total loss of engine power.
Probable Cause: The pilot’s improper preflight inspection during which he relied on the fuel totalizer and failed to ensure that sufficient fuel was onboard for the flight, which resulted in fuel exhaustion and a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN16LA381 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
26-Sep-2016 12:54 |
Aerossurance |
Added |
17-Oct-2016 20:01 |
Aerossurance |
Updated [Time, Phase, Departure airport, Source, Narrative] |
08-Sep-2017 19:48 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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