ASN Wikibase Occurrence # 193544
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Date: | Sunday 12 February 2017 |
Time: | 14:10 |
Type: | Cessna 172S Skyhawk |
Owner/operator: | Private |
Registration: | N2179L |
MSN: | 172S9633 |
Year of manufacture: | 2004 |
Total airframe hrs: | 8564 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 1 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Diego County, Pamo Valley NW of Ramona, CA -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | San Diego-Gillespie Field, CA (SEE/KSEE) |
Destination airport: | San Diego-Gillespie Field, CA (SEE/KSEE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane departed on an instructional flight with a flight instructor in the right front seat, a student pilot in the left front seat, and a passenger in the right rear seat. They completed maneuvers in a practice area, flew to a valley located in mountainous terrain, and performed a simulated engine failure maneuver. The flight instructor and the student pilot provided differing accounts of the events that followed the simulated engine failure maneuver. According to the flight instructor, after performing the simulated engine failure maneuver, the student pilot advanced the throttle to full power and turned east toward rising terrain. The flight instructor reported that the gauges all read normal, but the airplane would not outclimb the approaching terrain. He took over the controls but could not turn left or right due to the rising terrain on both sides of the airplane. According to the instructor, he had no choice but to crash the airplane.
According to the student pilot, the flight instructor told him to turn east towards the rising terrain and then took control of the airplane. The student reported that the flight instructor made a comment about demonstrating the airplane's performance, added full power, leaned the mixture, flew straight for 5 seconds, and then said an expletive shortly before the airplane crashed into a mountain.
Flight track data recovered from a personal electronic device onboard the airplane showed that, after the simulated engine failure maneuver, the airplane climbed and turned east entering terrain that rose in front and on both sides of the airplane. The track continued to climb for about 1 minute 5 seconds before reaching the accident site.
Postaccident examination of the airplane revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. According to the pilot's operating handbook for the airplane, at its maximum gross weight, under standard conditions, with no flaps and full throttle, the airplane was capable of climbing at a maximum rate of 625 ft per minute, at 73 knots indicated airspeed, at 2,000 ft mean sea level (msl).
The flight track data for the final 1 minute 5 seconds of the flight indicated that the airplane climbed about 584 ft, corresponding to a rate of climb slightly less than the published maximum rate of climb. During the climb, the left turn towards the east would have decreased the rate-of-climb performance, which likely accounts for the rate of climb being less than the published maximum.
During the impact sequence, a tree penetrated up through the center of the cabin floor just behind the front seats and exited through the cabin roof. The airplane came to rest upright. The instructor was able to unbuckle his seatbelt but had to cut the student pilot's seatbelt to free him. After examining the passenger, the instructor realized that her seatbelt was not latched and that her injuries were fatal.
The autopsy of the passenger determined her cause of death to be blunt force injuries of the head and neck. These injuries were likely due to impact with the tree that penetrated the cabin area.
Probable Cause: The flight instructor's failure to ensure that adequate clearance from terrain was maintained after performance of a simulated engine failure maneuver, which resulted in controlled flight into terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR17FA063 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N2179L
History of this aircraft
Other occurrences involving this aircraft
5 October 2014 |
N2179L |
Northern Arizona Investment Group LLC |
0 |
Sedona, Arizona |
|
sub |
Gear collapse |
Location
Images:
NTSB
Revision history:
Date/time | Contributor | Updates |
13-Feb-2017 01:29 |
Geno |
Added |
13-Feb-2017 01:37 |
Geno |
Updated [Operator, Total fatalities, Other fatalities, Departure airport, Source, Damage, Narrative] |
13-Feb-2017 20:59 |
Geno |
Updated [Aircraft type, Registration, Cn, Nature, Source] |
22-Mar-2019 19:09 |
ASN Update Bot |
Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
24-Mar-2019 08:39 |
harro |
Updated [Phase, Departure airport, Destination airport, Source, Narrative, Photo] |
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