ASN Wikibase Occurrence # 194756
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 5 April 2017 |
Time: | 14:10 |
Type: | Cessna T210M Turbo Centurion |
Owner/operator: | Private |
Registration: | N1215M |
MSN: | 21061924 |
Year of manufacture: | 1977 |
Total airframe hrs: | 5810 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Detroit Lakes Airport (KDTL), Detroit Lakes, MN -
United States of America
|
Phase: | Landing |
Nature: | Ferry/positioning |
Departure airport: | Moorhead, MN (JKJ) |
Destination airport: | Detroit Lakes, MN (DTL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot reported that, before the accident flight, the airplane had been experiencing intermittent landing gear problems and that the purpose of the flight was to bring the airplane to a maintenance facility to examine the landing gear system. He added that, before the flight, the landing gear circuit breaker was pulled out “in order to keep the gear in the down position and eliminate the gear warning horn” for the flight. While landing, the pilot noticed that the left wing slightly dropped after touchdown, and the pilot corrected with aileron to maintain the runway centerline. Shortly thereafter, the pilot could feel the right main landing gear (MLG) slowly collapse. The pilot was unable to maintain the airplane on the runway centerline, and the airplane exited the runway surface. The airplane came to rest upright with the right MLG collapsed, and the right horizontal stabilizer was bent.
During a postaccident examination, the landing gear were retracted and extended multiple times. Each gear retraction was normal; however, the gear extension cycles resulted in the left MLG and nose landing gear extending and locking, and the right MLG extending with no movement from the downlock actuator. The actuator was removed for further examination, and it was difficult to move. After removal, the actuator released, and the internal spring mechanism freely moved the actuator. The actuator was disassembled with no internal problems noted.
According to the Pilot’s Operating Handbook, Section 3, “Emergency Procedures, Landing Gear Malfunction Procedures,” the landing gear pump circuit breaker was to be positioned to the “in” position for all landing gear malfunction scenarios.
Probable Cause: The malfunction of the right main landing gear actuator for reasons that could not be determined because postaccident examination revealed no mechanical anomalies that would have precluded normal operation. Contributing to the accident was the improper decision to disengage the landing gear system circuit breaker before the flight, which was contrary to the manufacturer-recommended procedures.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA148 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=1215M
History of this aircraft
Other occurrences involving this aircraft
27 January 1994 |
N1215M |
J.p. Hunt |
0 |
Olathe, KS |
|
sub |
2 May 2021 |
N1215M |
Private |
1 |
Green Castle Airport (IA24), Oxford, IA |
|
w/o |
Collision with pole or wires |
Location
Revision history:
Date/time | Contributor | Updates |
11-Apr-2017 18:58 |
Geno |
Added |
19-Aug-2017 16:48 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation