ASN Wikibase Occurrence # 195921
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Date: | Sunday 4 June 2017 |
Time: | 08:24 |
Type: | Excalibur Aircraft Excalibur |
Owner/operator: | Private |
Registration: | N78DZ |
MSN: | 2614 |
Year of manufacture: | 2015 |
Total airframe hrs: | 64 hours |
Engine model: | Rotax 582UL-99 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bernalillo County, Albuquerque, NM -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Albuquerque-Double Eagle II Airport, NM (KAEG) |
Destination airport: | Albuquerque-Double Eagle II Airport, NM (KAEG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was conducting a personal flight in the experimental amateur-built airplane. After about 1 hour of flight, the airplane was straight and level, at an airspeed of about 75 mph, when the pitch control became erratic. The pilot stated that the control stick started “slamming” fore and aft to the limits, the airplane nose began pitching up and down, and the airplane began buffeting “like it was going to come apart.” The pilot declared an emergency and reduced airspeed to 50 to 60 mph, which slightly lessened the fore-and-aft stick movement and pitch but did not control it. The pilot turned to clear steep terrain and chose a field for an emergency landing. He was able to make final directional corrections and flew the airplane to landing about 40 to 45 mph and 200 to 300 ft per minute rate of descent. The left wing and horizontal stabilizer struck the ground. Examination of the airplane revealed a broken right elevator control rod; the left elevator control rod was not broken and moved normally. The broken control rod was a factory-supplied, 1/2-inch aluminum tube with bearings at each end. The attach points of the control rods appeared to be intact, the bearings were still connected and safety wired, and all other control rod linkages were connected. Further examination revealed no indication of any preexisting failure on the fracture surface of the right elevator control rod. The deformation of the rod was indicative of a bending failure. The pilot reported after the accident that he may have encountered flutter, but it could not be determined when or if that occurred.
Probable Cause: The loss of pitch control due to the overload failure of the control rod.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA216 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=78DZ Location
Revision history:
Date/time | Contributor | Updates |
04-Jun-2017 21:35 |
Geno |
Added |
19-Apr-2020 17:29 |
ASN Update Bot |
Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
19-Apr-2020 17:58 |
harro |
Updated [Aircraft type, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
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