ASN Wikibase Occurrence # 197256
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Date: | Wednesday 9 August 2017 |
Time: | 12:20 |
Type: | Cessna 172S Skyhawk |
Owner/operator: | Kcsi Texas Inc |
Registration: | N5274Q |
MSN: | 172S9199 |
Year of manufacture: | 2002 |
Total airframe hrs: | 6300 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Jackson County, NW of Wellston, OH -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Survey |
Departure airport: | Newark, OH (VTA) |
Destination airport: | Jackson, OH (I43) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot and observer were conducting an aerial observation flight of a pipeline. The pilot reported that, while maneuvering at a low altitude toward an airport to refuel, he heard a “significant boom” and noticed a reduction in engine rpm. The pilot unsuccessfully attempted to regain engine power and then initiated a forced landing to a space between trees. During the forced landing, the airplane impacted rolling, uneven grass terrain and a barbed wire fence.
Examination and disassembly of the engine revealed a large hole on the top of the engine crankcase inboard of the No. 4 cylinder. The examination revealed that the No. 4 connecting rod had failed due to the installation of a nonconforming small end connecting rod bushing. Five days before the accident, the engine manufacturer had issued a mandatory service bulletin indicating that the accident connecting rod bushing may not have met engine specifications and may require followup action. Six days after the accident, the Federal Aviation Administration issued an airworthiness directive that required inspecting the connecting rods, replacing affected connecting rod small end bushings, and accomplishing the instructions in the engine manufacturer’s mandatory service bulletin.
Probable Cause: The failure of a connecting rod small end bushing, which resulted in a loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA311 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=5274Q Location
Revision history:
Date/time | Contributor | Updates |
10-Aug-2017 05:53 |
Geno |
Added |
07-Feb-2018 13:47 |
ASN Update Bot |
Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative] |
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