Accident Cessna 177RG Cardinal RG N1528H,
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ASN Wikibase Occurrence # 198617
 
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Date:Friday 30 September 2016
Time:14:30
Type:Silhouette image of generic C77R model; specific model in this crash may look slightly different    
Cessna 177RG Cardinal RG
Owner/operator:Private
Registration: N1528H
MSN: 177RG0704
Year of manufacture:1975
Total airframe hrs:9668 hours
Engine model:Lycoming IO-360-A1B6D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Cloquet, MN -   United States of America
Phase: En route
Nature:Private
Departure airport:Cook, MN (CQM)
Destination airport:Hinckley, MN (04W)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during cruise flight, the airplane’s engine began making an unusual ticking sound and the oil pressure was low. The oil pressure continued to drop, and the engine began to “knock” louder until it experienced a total loss of power. The pilot attempted to glide to an airport, but the airplane had insufficient altitude and landed in a field short of the intended runway. Postaccident examination of the engine revealed that the No. 4 connecting rod had failed, and displayed signatures consistent with a lack of lubrication. The other connecting rods also exhibited signs of a lack of lubrication, and the oil pickup screen contained debris. The engine had sufficient oil in the sump, and examination of the components of the oil system failed to reveal any preimpact anomalies. The engine manufacturer recommended that engines be overhauled at least every 12 years due to possible deterioration of engine components and abnormal wear on soft metal bearing surfaces during engine start procedures. The accident engine had not been overhauled for 23 years; however, the investigation was unable to determine if or to what extent the damage to the engine was a result of the connecting rod failure or may have occurred before the failure.

Probable Cause: A lack of lubrication in the engine for reasons that could not be determined based on the available information, which resulted in a failure of the No. 4 connecting rod and a subsequent total loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN16LA391
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
19-Aug-2017 13:17 ASN Update Bot Added

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