ASN Wikibase Occurrence # 198650
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Date: | Thursday 23 July 2015 |
Time: | 18:00 |
Type: | Kinner B Sportster |
Owner/operator: | Private |
Registration: | NC13776 |
MSN: | 102 |
Year of manufacture: | 1934 |
Total airframe hrs: | 2000 hours |
Engine model: | KINNER B5 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Eagles Mere, PA -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Eagles Mere, PA (4PN7) |
Destination airport: | Eagles Mere, PA (4PN7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot reported that the airplane had undergone a complete restoration and had been flown for about 8 hours in the 9 months before the accident. He added that, about 1 week before the accident, the airplane experienced a loss of engine power on takeoff but that he was able to land the airplane without incident. A carburetor anomaly was found that appeared to have produced an overly rich mixture and was subsequently corrected.
On the day of the accident, an engine run was performed to verify that there were no operational issues. The pilot subsequently took off for the local personal flight, climbed the airplane to 50 ft above the runway, and then landed uneventfully. He then took off again, and when the airplane climbed to about 150 ft above the runway, the engine stopped, and the pilot then performed an off-airport forced landing. During the landing, the fuel tank ruptured, and the engine broke away from the fuselage. Subsequent examination of the airframe and engine revealed no evidence of any preimpact mechanical anomalies that would have precluded normal operation.
The weather conditions at the time of the accident were conducive to the formation of serious carburetor icing at glide power. The airplane had carburetor heat, but the pilot reported that he did not use it in flight or on the ground. Although the formation of carburetor icing was highly unlikely under a full-power takeoff, it could have formed during the low-power taxi and then broken off or melted due to the added engine heat from the higher takeoff power. However, with no substantive evidence that carburetor ice had formed, the reason for the loss of power could not be determined.
Probable Cause: The total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA15LA279 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 13:47 |
ASN Update Bot |
Added |
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