ASN Wikibase Occurrence # 199531
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 20 February 2017 |
Time: | 08:45 |
Type: | Thunder & Colt AX10-180S1 |
Owner/operator: | Private |
Registration: | N709TC |
MSN: | 2444 |
Year of manufacture: | 1993 |
Fatalities: | Fatalities: 0 / Occupants: 10 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Albuquerque, NM -
United States of America
|
Phase: | Approach |
Nature: | Executive |
Departure airport: | Albuquerque, NM |
Destination airport: | Albuquerque, NM |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot of the balloon was performing a local sightseeing flight. The balloon took off from a field, climbed, and drifted southeast. As the balloon approached an interstate, the pilot began a descent to land on a field near a university campus.
About 100 to 140 ft above ground level (agl), the balloon entered a rapid descent. The pilot applied maximum fuel to the burner system to arrest the descent; however, the descent continued. The pilot stopped the descent about 50 ft agl and the balloon began to climb again; upon reaching 75 ft agl, the balloon gondola contacted power lines. The contact caused electricity to arc through the gondola, severing two of the four suspension cables. The pilot “hand-removed” the power line from the gondola, applied heat to the burner system, and climbed away from the power lines. The pilot subsequently made an uneventful landing on a soccer field at the university about a mile away from the power lines.
The National Weather Service (NWS) surface analysis chart depicted a cold front, which was located immediately south of the area at the time of the accident and moving across the state. The front resulted in a shift of the prevailing wind to the north-northwest with an increasing pressure gradient behind the front. Some lifting would be associated ahead of the front and then would subside but wouldn’t be classified as strong downdrafts near the accident site. Though not conclusive, it is possible that the shifting wind and changing weather conditions could have affected the performance of the balloon, causing an increase in its descent rate during the pilot’s landing approach.
Probable Cause: The pilot’s delayed reaction to the balloon’s increased rate of descent during an attempted landing, which resulted in impact with a power line.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA118 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
08-Sep-2017 19:49 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation