ASN Wikibase Occurrence # 205765
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 13 May 2015 |
Time: | 09:30 |
Type: | Grumman G-164A Ag-Cat |
Owner/operator: | Richter Aviation Inc |
Registration: | N8875H |
MSN: | 1556 |
Year of manufacture: | 1975 |
Total airframe hrs: | 10031 hours |
Engine model: | Pratt & Whitney R1340-AN1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Maxwell, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Agricultural |
Departure airport: | Maxwell, CA (PVT) |
Destination airport: | Maxwell, CA (PVT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Just after takeoff on the agricultural application flight, the commercial pilot was positioning the airplane to spray a rice field. About 200 ft above ground level, the pilot heard a loud pop, and the engine experienced a total loss of power. The pilot turned the airplane to land on a dirt road, but it was too narrow; the right main landing gear contacted mud on the side of the road, and the airplane subsequently nosed over and came to rest inverted. Recovery personnel reported no residual fuel on the ground around the accident site, and about one half gallon of fuel was recovered from the airplane.
The pilot stated that the airplane had not been refueled on the day of the accident and that he departed on the flight with less than a half tank of fuel.
The postaccident engine examination revealed no mechanical anomalies that would have precluded normal operation. The loss of engine power was likely due to fuel exhaustion, and given that the loss of power occurred just after takeoff, it is likely that the pilot did not verify the amount of fuel onboard before departing on the flight.
Probable Cause: The pilot’s improper preflight inspection and fuel planning, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15LA160 |
Status: | Investigation completed |
Duration: | 2 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft
7 May 1999 |
N8875H |
Richter Aviation |
0 |
Maxwell, CA |
|
w/o |
Location
Revision history:
Date/time | Contributor | Updates |
07-Feb-2018 13:47 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation