Incident Rockwell Commander 114 VH-DDY,
ASN logo
ASN Wikibase Occurrence # 208420
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 30 October 1994
Time:16:05
Type:Silhouette image of generic AC11 model; specific model in this crash may look slightly different    
Rockwell Commander 114
Owner/operator:
Registration: VH-DDY
MSN: 14280
Year of manufacture:1977
Fatalities:Fatalities: 0 / Occupants:
Aircraft damage: Substantial
Location:Phillip Island, VIC -   Australia
Phase: Landing
Nature:Unknown
Departure airport:YMMB
Destination airport:YMMB
Investigating agency: BASI
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On arrival at Moorabbin the pilot asked a staff member the fuel state of the aircraft. The staff member said he thought it was full but for the pilot to check. The pilot said he checked the tanks visually during his pre-flight inspection and believed they were full. He could not recall what the fuel quantity gauges were indicating. Engine run-up prior to departure was normal. The fuel selector was selected to the BOTH position and was left at that position for the entire flight. The purpose of the flight was for the pilot to practise intercepts on the Cowes navigation aids. There was a safety pilot in the right seat whose task was to watch for traffic and to "keep an eye" on the pilot. The safety pilot was not familiar with the aircraft type. After completing the airwork and while preparing to return to Moorabbin, the engine gave a short miss. At this time the pilot said they were about five miles to the east of Phillip Island airstrip at an altitude of 3500 feet. Shortly afterwards the engine missed again. This missing then occurred at more frequent intervals. The pilot therefore decided to make a precautionary landing at Phillip Island. At this time the aircraft was still at 3500 feet and in a high wide base position for the 220 degree strip, which he decided to use. The pilot said he checked the magnetos, turned the electric fuel pump on, checked the mixture was rich and checked the fuel selector was in the BOTH position. He did not move the selector. Because the aircraft was high, the throttle was selected to the idle position and landing gear and full flap were extended. Some S turns were made on final approach to lose altitude but the aircraft still arrived over the strip far too high. At the upwind end of the strip the pilot pushed the throttle forward hoping there would be power available for a go around but there was no response from the engine. He then pulled the aircraft up into a left turn, to avoid going into the sea, and crash landed in sand dunes to the east of the airstrip. The investigation revealed that there was approximately 40 litres of fuel in the left tank but the right tank was probably empty. The right wing tank fuel lines had been severed in the accident so fuel could have escaped from these lines after the accident. However, when refuelling records were checked against known fuel usage, 40 litres was about what should have been remaining and that much was drained from the left tank. The tank filler necks on this aircraft are fitted with anti-syphon (flapper) valves which have to be depressed to visually check tank contents. The pilot did not depress those valves during his pre-flight inspection. After the wreckage was recovered. the entire fuel system was inspected and no faults were found. The engine was removed and placed in a test rig where it ran faultlessly through its entire power range.

Accident investigation:
cover
  
Investigating agency: BASI
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

https://www.atsb.gov.au/publications/investigation_reports/1994/aair/199403176/
https://www.atsb.gov.au/media/4934241/199403176.pdf

History of this aircraft

Other occurrences involving this aircraft
20 January 1986 VH-DDY 0 Sea Lake, VIC sub

Revision history:

Date/timeContributorUpdates
29-Mar-2018 12:46 Pineapple Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org