Accident Beechcraft A36 Bonanza N36LP,
ASN logo
ASN Wikibase Occurrence # 210581
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Friday 4 May 2018
Time:19:30
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Private
Registration: N36LP
MSN: E-894
Year of manufacture:1976
Total airframe hrs:7951 hours
Engine model:Continental IO-520-BB
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lafayette County, southeast Shullsburg, WI -   United States of America
Phase: Landing
Nature:Private
Departure airport:Okmulgee, OK (OKM)
Destination airport:Plainfield, WI (WN09)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot reported that he heard an unusual noise from the engine during cruise flight and shortly afterward, the engine experienced a total loss of power. The pilot performed a forced landing to an open field.

Visual examination of the engine revealed a hole in the crankcase. A teardown examination revealed fretting on the crankcase mating surfaces, shifting of the No. 2 main bearing within the journal support, thermal damage consistent with a loss of oil lubrication, and separation of the crankshaft. The observed fretting damage was consistent with relative movement of the crankcase halves during operation due to a lack of through-bolt torque. The main journal bearing damage, the separation of the crankshaft, and the crankcase damage were secondary and a result of the loss of lubrication.

An engine overhaul was completed in about 11 years 5 months before the accident; about 849 flight hours had accumulated since the overhaul. Two cylinders were replaced 6 years before the accident, and one cylinder was replaced during the most recent annual inspection about 9 months before the accident. It is likely that improper torque of the through-bolt nuts was applied during one of the cylinder replacement events, though it could not be determined which event.

Probable Cause: A catastrophic engine failure due to improper torque on the engine through-bolt nuts, which resulted in relative movement between the crankcase halves, damage to a main journal bearing, and a loss of oil lubrication.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN18LA159
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=36LP

https://flightaware.com/live/flight/N36LP

Location

Revision history:

Date/timeContributorUpdates
07-May-2018 13:52 Geno Added
07-May-2018 13:54 Geno Updated [Date]
01-Jun-2019 07:28 ASN Update Bot Updated [Aircraft type, Operator, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org