ASN Wikibase Occurrence # 222683
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Date: | Wednesday 6 March 2019 |
Time: | 14:00 LT |
Type: | Cessna 150F |
Owner/operator: | Private |
Registration: | N6917F |
MSN: | 15063517 |
Year of manufacture: | 1966 |
Total airframe hrs: | 4561 hours |
Engine model: | Continental O-200 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Burnet County, Granite Shoals, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Granite Shoals, TX (2G5) |
Destination airport: | San Marcos Regional Airport, TX (KHYI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he last fueled the airplane about 5 months before the accident. Before the flight, the pilot conducted a preflight inspection and sumped both wing fuel tanks. The left fuel tank had some sediment present, but as he continued sumping the fuel became clear. The fuel in the right fuel tank ran clear. After engine start, the left tank fuel gauge indicated near empty, and the right fuel tank gauge indicated about 1/4 full. Subsequently, the pilot took off for a personal cross-country flight. After starting a right turn, and about 600 ft above ground level, the engine sputtered and lost power. The pilot then attempted to turn back to the airport but realized that the airplane was too low, so he executed a forced landing to a field with small trees, during which the left wing struck a tree, which resulted in substantial damage to the wing.
The pilot reported that, after the accident, he found more sediment in the left tank. He stated that he believed that the low fuel state and the sediment in the left tank may have starved the engine of fuel during the turn and that having more fuel onboard would have 'probably been helpful.' However, it is more likely that, due to the low fuel state, when the pilot conducted the right turn, the fuel became unported, resulting in the loss of engine power due to fuel starvation.
Probable Cause: The pilot's decision to takeoff with a limited amount of fuel onboard, which unported during a turn, resulting in fuel starvation and a subsequent loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA101 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA101
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=6917F Location
Media:
Revision history:
Date/time | Contributor | Updates |
07-Mar-2019 02:56 |
Geno |
Added |
07-Mar-2019 03:11 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Nature, Source, Narrative] |
07-Mar-2019 08:44 |
Iceman 29 |
Updated [Source, Embed code] |
08-Mar-2019 09:21 |
RobertMB |
Updated [Registration, Source, Embed code] |
08-Jul-2022 18:31 |
ASN Update Bot |
Updated [Time, Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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