ASN Wikibase Occurrence # 22657
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 31 August 2008 |
Time: | 09:25 |
Type: | Piper PA-18-150 |
Owner/operator: | Van Wagner Aerial Media, LLC |
Registration: | N7482D |
MSN: | 18-5817 |
Year of manufacture: | 1957 |
Total airframe hrs: | 12118 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Camarillo, CA -
United States of America
|
Phase: | Take off |
Nature: | Banner and glider towing |
Departure airport: | Camarillo, CA (CMA) |
Destination airport: | Camarillo, CA (CMA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a banner pickup maneuver, witnesses observed the airplane level off from the descent about 150 feet before the banner pickup loop, then rotate and catch the banner pickup loop with its main landing gear instead of the tail hook. Witnesses stated that as the banner started to lift, the pilot added full power and began a climbout at a 45-degree angle to an altitude of about 150 feet. The airplane was then observed to level off before the nose suddenly dropped to about a 30-to-45-degree nose-down attitude before impacting the ground. One of the pilots who witnessed the accident said that it appeared that the pilot might be trying to land straight ahead but did not level off prior to ground impact. According to company procedures, the pilot is expected to establish an approach speed of 80 to 85 mph, maintaining a 15 degree to 20 degree approach angle until the rotation point at the banner pickup loop, and establish full power before rotating. Rotation serves to swing the hook down and forward to snag the rope, as opposed to a flat approach that drags the hook across the rope. As the airplane rotates, the nose is to be raised approximately 20 degrees to 30 degrees above the horizon. At 150 feet, the power is pulled back and the airplane smoothly leveled off at an altitude of 200 feet where full power is then applied. A postaccident examination noted no preimpact anomalies with the airframe or engine which would have precluded normal operation.
Probable Cause: The pilot's failure to fly the correct approach profile that resulted in the inadvertent pickup of a banner tow line with the airplane's main landing gear.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA08LA192 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
(c) NTSB
(c) NTSB
Revision history:
Date/time | Contributor | Updates |
02-Sep-2008 22:27 |
jorgetadeu7 |
Updated |
08-Jun-2009 12:10 |
harro |
Updated |
08-Jun-2009 12:14 |
harro |
Updated |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 11:58 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation