ASN Wikibase Occurrence # 30039
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Date: | Friday 1 September 2000 |
Time: | 14:50 |
Type: | Cessna 310G |
Owner/operator: | Private |
Registration: | N8978Z |
MSN: | 310G0078 |
Total airframe hrs: | 2357 hours |
Engine model: | Continental IO-470D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Seven Springs Airport, Seven Springs Borough, Pennsylvania -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Atlanta, GA (FFC) |
Destination airport: | Glens Falls, NY (GFL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While at 5,000 feet in VMC, the right engine spinner look unusual to the pilot. He reduced the throttle, but could not identify the problem, so he secured the engine. A tear in the spinner was identified. The pilot restarted the engine, but then shut it down because of a vibration. The pilot advised ATC that he had secured the engine, and needed to divert. While on short final, the pilot realized he would not make his intended touchdown point, because the airplane was too high. With the airplane 'sinking excessively,' the pilot decided to go around. He advanced the throttle on the left engine, the airplane rolled right, and then impacted trees. The right spinner had a 1/2-inch crack that started at its base and ran perpendicular to the rotation of the propeller. The crack then transitioned to a tear. The fracture surface for the crack was grayish in color, and consistent with fatigue. The POH stated that the pilot was to check the propeller and spinner for 'nicks, security and oil leaks,' prior to flight. The recommended safe single-engine speed for the airplane was 92 knots.
Probable Cause: The pilot's failure to maintain the manufacture's recommended safe single-engine airspeed, which resulted in a velocity-minimum-control roll to the right. A factor in the accident was the pilot's failure to maintain a proper glide path to his intended touchdown point, which resulted in a single engine go-around attempt.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC00LA246 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X22050&key=1 FAA register: 2.
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8978Z Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
12-Jun-2014 04:06 |
Dr. John Smith |
Updated [Time, Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 19:09 |
ASN Update Bot |
Updated [Cn, Total occupants, Departure airport, Destination airport, Source, Narrative] |
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