Accident Bellanca 17-31A Super Viking 300A N8855V,
ASN logo
ASN Wikibase Occurrence # 35034
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 16 March 1983
Time:23:30
Type:Silhouette image of generic BL17 model; specific model in this crash may look slightly different    
Bellanca 17-31A Super Viking 300A
Owner/operator:private
Registration: N8855V
MSN: 32-49
Total airframe hrs:1675 hours
Engine model:LYCOMING IO-540-K1E5
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Waverly, GA -   United States of America
Phase: Approach
Nature:Training
Departure airport:Chamblee, GA (PDK)
Destination airport:Saint Simons Id, GA (SSI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE ACFT CRASHED INTO TREES DURING AN INSTRUMENT APPROACH AT NIGHT IN STORMY WEATHER. BOTH THE CFI, SEATED IN THE FRONT LEFT SEAT, & THE NEW OWNER OF THE ACFT, WERE FATALLY INJURED. AN IFR FLT PLAN WAS FILED & THE CFI HAD OBTAINED 2 WX BRIEFINGS PRIOR TO DEPARTURE. THE ACFT HAD JUST RECEIVED AN ANNUAL INSPECTION AS A PART OF THE SALES CONTRACT. AT 2313 BRUNSWICK FSS ADVISED JACKSONVILLE CENTER THAT N8855V WAS CLEARED FOR APPROACH & WAS INBOUND. JACKSONVILLE GAVE FSS THE MISSED APPROACH PROCEDURES. AT 2321 FSS ADVISED JACKSONVILLE THAT COMMUNICATIONS HAD BEEN LOST. INVESTIGATION REVEALED THAT ALTHOUGH THE ACFT HAD RECEIVED AN ANNUAL INSPECTION ON 03-15-83, A DISCREPANCY LIST, DATED 03-16-83, FOUND IN THE ACFT SHOWED THE #2 VOR WAS UNRELIABLE; THE DIRECTIONAL GYRO PRECESSED; THE COMPASS NEEDED TO BE CALIBRATED; THE FUEL GAUGES WERE UNRELIABLE; & THE ALTERNATOR OUTPUT WAS SUSPECT IN HIGH LOAD SITUATIONS. THE ALTIMETER, PITOT STATIC SYSTEM & TRANSPONDER HAD NOT BEEN RECERTIFIED SINCE 1978. ALSO, NO RECORD OF VOR ACCURACY CHECKS WERE FOUND DURING THE INVEST. CAUSE:

Sources:

NTSB: https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X42334

History of this aircraft

Other occurrences involving this aircraft
17 March 1983 N8855V Private Waverly, GA w/o

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org