ASN Wikibase Occurrence # 35283
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Date: | Saturday 15 October 1994 |
Time: | 17:28 |
Type: | Piper PA-32-300 Cherokee Six |
Owner/operator: | Sanitors Southwest |
Registration: | N2964A |
MSN: | 32-7940231 |
Total airframe hrs: | 3405 hours |
Engine model: | LYCOMING IO-540-K1G5D |
Fatalities: | Fatalities: 1 / Occupants: 5 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | College Station, TX -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Easterwood Airport, TX (CLL/KCLL) |
Destination airport: | San Antonio International Airport, TX (SAT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On October 15, 1994, at 1728 central daylight time, a Piper PA-32-300, N2964A, was destroyed following a loss of control near College Station, Texas. The private pilot and one of his passengers received minor injuries, two passengers were seriously injured, and one passenger sustained fatal injuries. Visual meteorological conditions prevailed for the personal flight.
THE FORWARD BAGGAGE COMPARTMENT DOOR CAME OPEN AND BEGAN 'FLAPPING' DURING TAKEOFF ROLL/INITIAL TAKEOFF CLIMB. THE PILOT CONTINUED HIS TAKEOFF AND RADIOED THAT HIS BAGGAGE COMPARTMENT DOOR HAD POPPED OPEN AND HE WAS RETURNING TO LAND. THE AIRPLANE WAS OBSERVED FLYING IN A STEEP CLIMB ATTITUDE, AT VERY SLOW AIRSPEED, IN A PRONOUNCED LEFT CRAB OR SLIP, IN A LEFT TURN AT AN ALTITUDE OF APPROXIMATELY 75 TO 100 FEET. THE PASSENGER IN THE RIGHT FRONT SEAT REPORTED HEARING THE STALL WARNING HORN INTERMITTENTLY PRIOR TO THE AIRPLANE'S IMPACT WITH TWO UTILITY POLES. THE PILOT REPORTED THAT HE HAD TAKEN A QUART OF OIL FROM THE FORWARD BAGGAGE COMPARTMENT TO REPLENISH THE ENGINE OIL. HE REPORTED THAT HE DID NOT REMEMBER IF THE TOP PART OF THE LATCH WAS LATCHED PRIOR TO HIS TAKEOFF. EXAMINATION OF THE AIRCRAFT AND ENGINE DID NOT DISCLOSE ANY MECHANICAL PROBLEMS.
Probable Cause: THE PILOT'S FAILURE TO MAINTAIN AIRSPEED AND THE RESULTING INADVERTENT STALL. FACTORS WERE THE PILOT'S INADEQUATE PREFLIGHT INSPECTION, AND HIS DIVERTED ATTENTION TO AN OPEN CARGO DOOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW95FA019 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001206X02427 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Oct-2022 05:26 |
Captain Adam |
Updated [Aircraft type, Departure airport, Destination airport, Narrative, Accident report] |
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