Accident Piper PA-32-300 Cherokee Six N2964A,
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ASN Wikibase Occurrence # 35283
 
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Date:Saturday 15 October 1994
Time:17:28
Type:Silhouette image of generic PA32 model; specific model in this crash may look slightly different    
Piper PA-32-300 Cherokee Six
Owner/operator:Sanitors Southwest
Registration: N2964A
MSN: 32-7940231
Total airframe hrs:3405 hours
Engine model:LYCOMING IO-540-K1G5D
Fatalities:Fatalities: 1 / Occupants: 5
Aircraft damage: Destroyed
Category:Accident
Location:College Station, TX -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Easterwood Airport, TX (CLL/KCLL)
Destination airport:San Antonio International Airport, TX (SAT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On October 15, 1994, at 1728 central daylight time, a Piper PA-32-300, N2964A, was destroyed following a loss of control near College Station, Texas. The private pilot and one of his passengers received minor injuries, two passengers were seriously injured, and one passenger sustained fatal injuries. Visual meteorological conditions prevailed for the personal flight.

THE FORWARD BAGGAGE COMPARTMENT DOOR CAME OPEN AND BEGAN 'FLAPPING' DURING TAKEOFF ROLL/INITIAL TAKEOFF CLIMB. THE PILOT CONTINUED HIS TAKEOFF AND RADIOED THAT HIS BAGGAGE COMPARTMENT DOOR HAD POPPED OPEN AND HE WAS RETURNING TO LAND. THE AIRPLANE WAS OBSERVED FLYING IN A STEEP CLIMB ATTITUDE, AT VERY SLOW AIRSPEED, IN A PRONOUNCED LEFT CRAB OR SLIP, IN A LEFT TURN AT AN ALTITUDE OF APPROXIMATELY 75 TO 100 FEET. THE PASSENGER IN THE RIGHT FRONT SEAT REPORTED HEARING THE STALL WARNING HORN INTERMITTENTLY PRIOR TO THE AIRPLANE'S IMPACT WITH TWO UTILITY POLES. THE PILOT REPORTED THAT HE HAD TAKEN A QUART OF OIL FROM THE FORWARD BAGGAGE COMPARTMENT TO REPLENISH THE ENGINE OIL. HE REPORTED THAT HE DID NOT REMEMBER IF THE TOP PART OF THE LATCH WAS LATCHED PRIOR TO HIS TAKEOFF. EXAMINATION OF THE AIRCRAFT AND ENGINE DID NOT DISCLOSE ANY MECHANICAL PROBLEMS.

Probable Cause: THE PILOT'S FAILURE TO MAINTAIN AIRSPEED AND THE RESULTING INADVERTENT STALL. FACTORS WERE THE PILOT'S INADEQUATE PREFLIGHT INSPECTION, AND HIS DIVERTED ATTENTION TO AN OPEN CARGO DOOR.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW95FA019
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001206X02427

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:22 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
12-Oct-2022 05:26 Captain Adam Updated [Aircraft type, Departure airport, Destination airport, Narrative, Accident report]

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