Accident Beechcraft B55 Baron N47SM,
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ASN Wikibase Occurrence # 35393
 
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Date:Monday 27 January 1997
Time:21:10 LT
Type:Silhouette image of generic BE55 model; specific model in this crash may look slightly different    
Beechcraft B55 Baron
Owner/operator:Donald L. Fenton Jr.
Registration: N47SM
MSN: TC-775
Total airframe hrs:4474 hours
Engine model:Continental IO-470-L
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Mayhill, NM -   United States of America
Phase: En route
Nature:Executive
Departure airport:Goodyear, AZ (KGYR)
Destination airport:Roswell, NM (KROW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The outboard portion of the right wing of the twin engine airplane impacted a pine tree in mountainous terrain during a night cross country flight. About 12 minutes prior to the accident, while 49 miles short of their intermediate destination, the pilot reported picking up ice at 9,500 feet MSL and reported that he was diverting to El Paso. ATC granted the frequency change to El Paso; however, no further radio calls were received. At 2005, a witness near the accident site, reported hearing the airplane flying at 'tree top level over his house' on a southeast direction. He stated that a low ceiling prevailed, the temperature was just above freezing and snow flurries restricted his visibility. Witnesses traveling on a gravel road adjacent to the accident site reported the lights of the airplane flying at tree top level prior the crash. The auxiliary fuel cell for the right engine was compromised by the initial collision with the pine tree and the 3 remaining tanks were destroyed by post-impact fire. Both fuel selectors were found in the AUX position. No discrepancies were found that would have prevented normal operations. The pilot had accumulated 7.5 hours of flight within the last 12 hours.

Probable Cause: The pilot's failure to maintain clearance with trees and terrain. Factors were the mountainous terrain, the snow obscuring the visibility, the dark night illumination, and the pilot's fatigue.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW97FA092
Status: Investigation completed
Duration: 2 years and 4 months
Download report: Final report

Sources:

NTSB FTW97FA092

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:22 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Jun-2023 04:03 Ron Averes Updated [[Time, Damage, Category, Investigating agency]]
08-Apr-2024 17:02 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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