ASN Wikibase Occurrence # 36002
Last updated: 19 June 2013
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| Date: | 23-OCT-1994 |
| Time: | 1503 |
| Type: |  Piper PA-23-250 |
| Operator: | private |
| Registration: | N999BW |
| C/n / msn: | 27-3242 |
| Fatalities: | Fatalities: 2 / Occupants: 2 |
| Other fatalities: | 0 |
| Airplane damage: | Written off (damaged beyond repair) |
| Location: | Newville, AL -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Dothan, AL (DHN) |
| Destination airport: | Jonesboro, GA (NONE) |
Narrative:MAINTENANCE HAD BEEN PERFORMED ON THE ENGINE TURBO-CHARGERS & EXHAUST SYSTEMS SEVERAL DAYS BEFORE THE ACCIDENT FLIGHT. AFTER DEPARTURE, THE PILOT REPORTED THAT THE LEFT ENGINE LOST POWER & HE ELECTED TO RETURN TO THE AIRPORT. A WITNESS REPORTED SEEING THE AIRPLANE HEADING TOWARD THE AIRPORT WITH AN ORANGE GLOW UNDER THE LEFT WING ABOUT FOUR FEET OUTBOARD OF THE FUSELAGE. THE WITNESS SAID THERE WAS A LOUD POP, THE LEFT WING SEPARATED FROM THE AIRPLANE, & THE PLANE FELL TO THE GROUND. INSPECTION REVEALED EXTENSIVE FIRE DAMAGE IN THE AREA OF THE LEFT WHEEL WELL & SPAR, BEHIND THE FIREWALL, IMMEDIATELY AFT OF THE TURBO-CHARGER EXHAUST. FUEL LINES IN THE WHEEL WELL AREA HAD BURNED AWAY. THE LEFT ENGINE TURBOCHARGER TAIL PIPE & MARMON CONNECTOR CLAMP WERE MISSING. THE ENGINES HAD BEEN EQUIPPED WITH AIRESEARCH TURBOCHARGERS IN ACCORDANCE WITH STC SA909WE. CAUSE: FAILURE OF MAINTENANCE PERSONNEL TO PROPERLY INSTALL THE MARMON CLAMP ON THE DISCHARGE SIDE OF THE TURBOCHARGER.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001206X02374
Revision history:| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
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