Accident Mooney M20E N2709W,
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ASN Wikibase Occurrence # 36257
 
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Date:Monday 22 June 1998
Time:12:00 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20E
Owner/operator:Stephen T. Gore
Registration: N2709W
MSN: 1020
Year of manufacture:1956
Total airframe hrs:3392 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 1 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Pickens, SC -   United States of America
Phase: En route
Nature:Private
Departure airport:Greenville, SC (KGYH)
Destination airport:Morristown, TN (MOR
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While in radio and radar contact with FAA Greenville/Spartanburg's Departure Control, climbing through 7,900 feet msl, to an assigned altitude of 9,500 feet msl, about 30 miles northwest of the Greenville/Spartanburg Airport, the pilot radioed that she had a very rough running engine and wanted vectors to the nearest airport. The controller supplied vectors to within 7 miles of the nearest airport, at which time the pilot chose a farmers field for a forced landing. The airplane collided with two pine trees within a stand of pines about 40 feet above ground, in a relatively flat, wings level, upright attitude. The airplane continued airborne for about 310 feet over a relatively clear field and then impact dense brush and 8- to 12-foot trees in an inverted attitude. Subsequent disassembly and examination of the engine and its associated components revealed no cause for the rough running engine. A finding of 0.056 ug/ml (ug/g) Diphenhydramine (antihistamine) was reported in the toxicological evaluation of the pilot's blood and urine.

Probable Cause: A loss of engine power for undetermined reasons and the pilot not maintaining adequate clearance with objects (trees) during the emergency landing. Contributing factors were the pilot's impairment associated with the use of an antihistamine and the trees.

Accident investigation:
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Investigating agency: NTSB
Report number: MIA98FA187
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB MIA98FA187

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:22 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Apr-2024 10:22 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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