Accident Lake LA-250 Renegade N14001,
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ASN Wikibase Occurrence # 36341
 
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Date:Monday 4 January 1999
Time:13:17 LT
Type:Silhouette image of generic LA25 model; specific model in this crash may look slightly different    
Lake LA-250 Renegade
Owner/operator:David L. Penney
Registration: N14001
MSN: 6
Engine model:Lycoming IO-540
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Laconia, NH -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Laconia, NH (KLCI)
Destination airport:Manchester, NH
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot/owner, sitting in the left seat, and flight instructor were on an instructional instrument flight. Shortly after takeoff, the airplane was seen trailing smoke. The smoke and engine noise stopped, then started again as the airplane leveled off, and began a left, 180-degree turn. The smoke and engine noise again stopped. Then the airplane descended, impacted a parking lot in a left-wing-down attitude, and bounced through a snow bank and down a 15-foot embankment, onto a field. It then rolled upside down, and caught on fire. A large hole was in the top of the engine crankcase, in line with a dislodged number 4 connecting rod. A hole in the bottom of the case was in line with a dislodged number 5 connecting rod. The number 1 connecting rod bearing and journal had light distress scoring in line with the oil supply hole. The number 2 connecting rod bearing and journal were normal, except for fire and heat damage to the bearing. The number 3, 4, 5, and 6 connecting rod journals had heavy distress scoring with extruded bearings. The injuries sustained by the pilot/owner precluded any recollection of the flight. He was not known to preheat the engine, and there were no witnesses to the airplane's preflight, start, runup or takeoff. Outside air temperature was 23 degrees Fahrenheit, and the airplane was stored in an unheated hangar. Recommended time between engine overhaul was 2,000 hours, or 12 years, which ever came first. The engine had in excess of 919 hours of operation, was built over 15 years earlier, and had not had an overhaul.

Probable Cause: A loss of engine power during initial climb due to oil starvation. Contributing to the accident was the failure to perform an engine overhaul.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: IAD99FA025
Status: Investigation completed
Duration: 1 year and 11 months
Download report: Final report

Sources:

NTSB IAD99FA025

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
25-Nov-2017 12:48 ASN Update Bot Updated [Cn, Operator, Departure airport, Destination airport, Source, Narrative]
14-Dec-2017 16:55 ASN Update Bot Updated [Cn, Operator, Departure airport, Destination airport, Narrative]
08-Apr-2024 11:08 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Accident report]

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