ASN Wikibase Occurrence # 36798
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Date: | Tuesday 5 August 1997 |
Time: | 13:48 LT |
Type: | Piper PA-28RT-201 |
Owner/operator: | Brett R. Allen |
Registration: | N8227Q |
MSN: | 28R-8018081 |
Total airframe hrs: | 4480 hours |
Engine model: | Lycoming IO-360-C1C6 |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hesperia, CA -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | San Jose, CA (KMRY) |
Destination airport: | (L26) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Following a go-around in high density altitude conditions, the airplane was observed to enter a shallow climb. It then turned approximately 20 degrees to the right and followed a wide depression in the surrounding terrain without any noticeable gain in altitude. While following this depression, three packages (luggage) were observed being thrown from the right side of the aircraft. After the third package was thrown, the aircraft flew into high voltage power lines, which ran perpendicular to the depression at an altitude of approximately 75 to 100 feet agl. The aircraft then impacted the ground and was destroyed by fire. There were no orange balls or other visually alerting devices attached to the power lines, as the power lines were not in a location normally used by low flying aircraft. A teardown inspection of the engine did not disclose any mechanical malfunction or abnormal wear; however, the exhaust muffler for the No. 2 and No. 4 cylinders had a partially collapsed internal baffle. Density altitude was about 7,200 feet. Aircraft performance charts indicated that at that altitude, the engine would have been developing only 72 percent of its rated power.
Probable Cause: failure of the pilot to see-and-avoid high voltage power lines, while coping with a lack of engine power during a go-around in a high density altitude condition. Factors relating to the accident were: high density altitude that resulted in a normal reduction of engine power; partial obstruction in the exhaust system that resulted in an additional loss of power; and the encounter with power lines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX97FA272 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX97FA272
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 13:40 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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