Accident Bellanca 17-30A Super Viking 300A N28049,
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ASN Wikibase Occurrence # 36884
 
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Date:Saturday 25 November 1995
Time:19:19 LT
Type:Silhouette image of generic BL17 model; specific model in this crash may look slightly different    
Bellanca 17-30A Super Viking 300A
Owner/operator:John G. Pfiitze
Registration: N28049
MSN: 78-30888
Engine model:Continental IO-520-K1B
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Kings Bay, GA -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Manville, NJ (47N)
Destination airport:Jacksonville, FL (JAX
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About 1745, while over Hilton Head airport en route to the pilot's planned fuel stop, the passenger/pilot's wife, using a cellular phone, reported to a friend that her husband couldn't descend below the clouds. At 1817, the pilot advised Jacksonville tower that the flight was about 22 miles northeast inbound for landing. One minute later he contacted Jacksonville approach and advised that he would '...get a little bit oriented first,...10 miles east-northeast inbound landing, circle around out here and get a heading or give me vector.' The airplane was assigned a discreet transponder code and the pilot was given the altimeter setting, wind information, and the active runway information. There was no further radio contact with the pilot. Radar data indicates that the airplane began a left descending turn to the east with the ground speed increasing. The airplane impacted the water during a descending left turn and the engine was heard to be operating normally. Examination of the recovered wreckage revealed evidence consistent with a high speed impact with the water.

Probable Cause: a loss of control due to pilot spatial disorientation. Contributing to the accident was: the dark night condition and the pilot's improper decision to turn to an easterly heading with no ground reference lights available.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA96LA029
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB MIA96LA029

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 10:52 ASN Update Bot Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, Category, Accident report]

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