ASN Wikibase Occurrence # 36885
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Date: | Friday 23 June 1995 |
Time: | 09:16 |
Type: | Beechcraft 58 Baron |
Owner/operator: | Air Orlando Charter |
Registration: | N4403Q |
MSN: | TH-809 |
Year of manufacture: | 1977 |
Total airframe hrs: | 6109 hours |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Orlando, FL -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | (ORL) |
Destination airport: | Jacksonville, FL (JAX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER TAKEOFF ON RWY 7, THE PILOT REPORTED TO FAA CONTROLLERS HE HAD AN ENGINE FAILURE. THE CONTROLLERS OBSERVED THE LANDING GEAR RETRACT AT THIS TIME AND THEN IMMEDIATELY EXTEND. WITNESSES OBSERVED THE ACFT AT TREE TOP LEVEL MAKING A TURN TO THE NORTH WITH THE LANDING GEAR DOWN AND THE LEFT ENGINE SHUTDOWN AND THE PROPELLER FEATHERED. THE ACFT DESCENDED AND STRUCK THE TOP OF A TREE WITH THE WINGS LEVEL. THE ACFT THEN ROLLED TO THE RIGHT 90 DEGREES AND STRUCK THE GROUND. THE ACFT THEN CARTWHEELED AND SLID BACKWARDS INTO A TREE WHERE IT CAME TO REST. EXAMINATION OF THE LEFT ENGINE SHOWED THE ENGINE DRIVEN FUEL PUMP DRIVE COUPLING WAS ROUNDED OFF AND NOT TURNING THE PUMP. THE DRIVE COUPLING WAS TOO SHORT FOR THE MODEL FUEL PUMP DRIVE SHAFT. A 1993 FAA AIRWORTHINESS DIRECTIVE THAT CALLS FOR CHECKING FOR THE PROPER LENGTH DRIVE COUPLING HAD NOT BEEN COMPLIED WITH. THE FLIGHT MANUAL FOR THE ACFT STATES THAT THE FIRST ACTION TO BE PERFORMED BY THE PILOT AFTER ENGINE FAILURE IS TO RAISE THE LANDING GEAR. THE MANUAL ALSO STATES THAT SINGLE ENGINE PERFORMANCE IS PREDICATED ON THE LANDING GEAR BEING RETRACTED. CAUSE: THE FAILURE OF THE PILOT-IN-COMMAND TO INSURE THE LANDING GEAR WAS RETRACTED FOLLOWING LOSS OF POWER IN ONE ENGINE RESULTING IN THE AIRCRAFT BEING UNABLE TO CLIMB AND CLEAR TREES IN THE AIRCRAFT'S FLIGHT PATH.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001207X03766 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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