Accident Mooney M20K N251BD,
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ASN Wikibase Occurrence # 37471
 
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Date:Sunday 23 January 2000
Time:18:53
Type:Silhouette image of generic M20T model; specific model in this crash may look slightly different    
Mooney M20K
Owner/operator:Private
Registration: N251BD
MSN: 25-0364
Engine model:Continental TSIO-360-LB1
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Pendleton, OR -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Pendelton, OR (PDT)
Destination airport:Eugene, OR (EUG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After landing to refuel, the pilot made an inadequate effort to remove airframe ice and snow, which had accumulated while on the ground before departing for his final destination. A witness (refueler) observed that about a half inch of somewhat moist snow had accumulated on the wings of the airplane prior to the time he fueled the airplane, necessitating brushing snow away from the fuel caps. The witness (refueler) stated that after wiping the snow off, there was still a covering of rough ice on the upper surface of the wing. During the fueling, he noticed that none of the ice on the wing had melted (ambient temperature at the time of the accident was minus 1 degree Celsius). The witness (refueler) also reported that after refueling the airplane, he looked at the right wing leading edge and pointed out some rough ice behind the area that the pilot had cleared, both on top and bottom of the wing. The pilot had rubbed his hand over the rough area, commenting that there wasn't enough ice to make any difference, before attempting his takeoff. The airplane crashed within two miles of the airport. The pilot's last radio communication received was that he was 'going down.' Post-crash examination of the engine revealed no evidence of pre-impact malfunction.
Probable Cause: The pilot's failure to adequately remove ice and snow from the airplane. A contributing factor was the pilot's inability to maintain control during climb due to degradation of the airplane's aerodynamic performance.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA00FA039
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X20431&key=1

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
12-Dec-2017 18:17 ASN Update Bot Updated [Operator, Source, Narrative]

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