ASN Wikibase Occurrence # 37542
Last updated: 24 May 2013
This information is added by users of ASN. ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.
Date:03-MAR-1984
Time:245
Type:Piper PA-28-236
Operator:private
Registration: N8054E
C/n / msn: 288211024
Fatalities:Fatalities: 2 / Occupants: 2
Other fatalities:0
Airplane damage: Written off (damaged beyond repair)
Location:Oconto, NE -   United States of America
Phase: En route
Nature:Private
Departure airport:Des Moines, IA (DSM)
Destination airport:Kearney, NE (EAR)
Narrative:
AFTER ATTENDING A BUSINESS CONFERENCE AT MUNCIE, IN, THE PLT RECEIVED A WX BRIEFING & TOOK OFF AT 2026 CST ON A FLT TO DES MOINES, IA, WHERE HE REFUELED. IN A PHONE CALL TO HIS WIFE AT THEIR HOME IN NORTH PLATTE, NE, HE INDICATED THE WX WAS SUCH THAT HE WOULD SPEND THE NIGHT AT DES MOINES. HOWEVER, AFTER CALLS TO THE FSS, HE ELECTED TO CONTINUE TO LINCOLN, NE. WHILE EN ROUTE, THE PLT REQUESTED THE GRAND ISLAND & NORTH PLATTE WX & WAS ADVISED THAT THEY WERE 25000 FT THIN BROKEN WITH UNRESTRICTED VISIBILITY.AT 0121 CST, HE EXTENDED HIS FLT PLAN TO PROCEED TO NORTH PLATTE. HE CONTINUED CHECKING ON THE CURRENT NORTH PLATTE WX. AT APRX 0218 CST, HE WAS ADVISED IT HAD DETERIORATED(CEILING 700 FT). A SHORT TIME LATER, THE CEILING DROPPED TO 600 FT OVERCAST. THE PLT DIVERTED TOWARD KEARNEY, NE, BUT THE ACFT DID NOT ARRIVE. AN INVESTIGATION REVEALED THAT IT HAD CRASHED IN A LEFT WING LOW, NOSE DOWN ATTITUDE. NO PREIMPACT PART FAILURE OR MALFUNCTION WAS FOUND. REPORTEDLY, THE PLT HAD NOT OBTAINED AN IN-DEPTH WX BRIEFING. CAUSE:

Sources:
NTSB: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X39118


Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
Number of views: 553

Corrections or additions? ... Edit this accident description