Accident Beechcraft A36 Bonanza N2558W,
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ASN Wikibase Occurrence # 38781
 
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Date:Thursday 25 April 1996
Time:12:09 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Richard A. Williford
Registration: N2558W
MSN: E-2306
Total airframe hrs:1060 hours
Engine model:Continental IO-550-B1
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Oklahoma City, OK -   United States of America
Phase: Landing
Nature:Private
Departure airport:Tulsa, OK (KTUL)
Destination airport:(2EJ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot called a fixed base operator (FBO) on Unicom frequency about 10 miles from the airport (Expressway Airpark). He was informed that the winds were 'out of the north, favoring runway 02.' Later, the pilot was heard to announced a 'go-around from runway 20.' The FBO told the pilot that he was 'trying to land downwind, use runway 02' to which the pilot replied 'OK.' The pilot made another call 'going around at Expressway.' A flight instructor contacted the pilot and notified him that he was using the wrong runway. The pilot's reply was unclear. The pilot next reported on a 'left downwind for 02.' The FBO corrected the pilot and told him 'you are upwind, the winds are from the north, preferred runway is 02' to which the pilot replied 'runway zero two.' On the third approach, the airplane touched down beyond the midpoint of runway 20. After rolling for a few feet, the pilot applied power and the airplane climbed to approximately 50 feet above the ground. The landing gear and flaps were retracted as the airplane assumed an exaggerated nose high climb attitude. Witnesses reported that the airplane was 'waffling' as it continued southbound. Subsequently, the pilot lost control of the airplane, and it impacted the ground.

Probable Cause: the pilot's delay in aborting the landing and his failure to obtain/maintain sufficient airspeed during the aborted landing, which resulted in an inadvertent stall and collision with the terrain. Factors relating to the accident were: the pilot's improper interpretation of the recommended landing runway, his selection of the wrong runway, and the resultant tailwind.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW96FA181
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB FTW96FA181

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 07:18 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report]

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