ASN Wikibase Occurrence # 38863
Last updated: 20 June 2013
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| Date: | 18-JAN-1991 |
| Time: | 1430 |
| Type: |  Beechcraft 35 Bonanza |
| Operator: | private |
| Registration: | N4589V |
| C/n / msn: | D-1060 |
| Fatalities: | Fatalities: 1 / Occupants: 2 |
| Other fatalities: | 0 |
| Airplane damage: | Written off (damaged beyond repair) |
| Location: | Arden, NC -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | (AVL) |
| Destination airport: | Lawrenceville, GA (17A) |
Narrative:DURING THE INITIAL CLIMB AFTER TAKEOFF, THE ENG LOST POWER. SUBSEQUENTLY, THE ACFT COLLIDED WITH TREES AND CRASHED. WATER WAS FOUND IN A FUEL LINE (BTN THE FUEL SELECTOR VLV AND ELECTRIC FUEL PUMP), ELECTRIC BOOST PUMP MANIFOLD, AND CARBURETOR (CARB) INLET STRAINER; HOWEVER, THE FUEL SYSTEM WAS DAMAGED DURING IMPACT AND FIRE SUPPRESSANT CHEMICALS WERE SPRAYED ON THE WRECKAGE. A CHECK OF THE CARB SHOWED THAT IT WAS PROVIDING A LEAN MIXTURE AT LOW POWER SETTINGS AND A RICH MIXTURE AT HI POWER SETTINGS. A TEARDOWN OF THE CARB REVEALED A CRYSTALLINE SUBSTANCE ON THE CARB DIAPHRAGM, AN IMPROPER METERING JET, AND THAT 5 SHIMS WERE INSTALLED IN THE CARB REGULATOR DIAPHRAGM SPRING MECHANISM. THE BENDIX OVERHAUL MANUAL ALLOWED A MAXIMUM OF 2 SHIMS. DURING A POST-ACDNT CHECK, THE ENG OPERATED NORMALLY WITH THE ELECTRIC FUEL PUMP ON, BUT THE ENG STOPPED RUNNING WHEN THE ELECTRIC PUMP WAS TURNED OFF. CAUSE: FOR UNDETERMINED REASONS, THE ENGINE LOST POWER.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X16256
Revision history:| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
Number of views: 741