Accident Cessna 152 N49205,
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ASN Wikibase Occurrence # 38893
 
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Date:Thursday 27 February 1997
Time:19:30 LT
Type:Silhouette image of generic C152 model; specific model in this crash may look slightly different    
Cessna 152
Owner/operator:Djms Inc.
Registration: N49205
MSN: 15281192
Year of manufacture:1977
Total airframe hrs:6718 hours
Engine model:Lycoming O-235-L2C
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Plaquemine, LA -   United States of America
Phase: En route
Nature:Training
Departure airport:Lafayette, LA (KLFT)
Destination airport:Reserve, LA (0LA4)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Approach Control was communicating with the pilot approximately 5 minutes prior to the accident and was providing VFR flight following through the Baton Rouge area. They reported that the pilot did not report any abnormalities with the aircraft. According to FAA records, the pilot got weather briefings from Automated Flight Service Stations before and during the flight. According to seven witness observations of people who were working on a levee adjacent to the accident site, the aircraft was in level flight, cruising over the Mississippi river at a low altitude beneath low clouds. One witness recalled seeing the aircraft approach high tension power lines which were traversing the river and perpendicular to the flight path. The aircraft impacted the lines, became hung up momentarily, and then fell into the river. Five of the witnesses heard the sound of an engine prior to the wire impact. The 2 power line support structures were 425 feet in height. Examination of the wreckage revealed wire strike marks beneath the right wing near the wing support strut attachment point. Throttle and mixture levers were both full forward and the tachometer needle was found at 2,500 RPM.

Probable Cause: The pilot's failure to maintain proper altitude and clearance from transmission wires. Factors were, the dark night, low cloud ceiling, and fog.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW97LA110
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

NTSB FTW97LA110

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Apr-2024 16:43 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report]

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