Accident Druine Turbulent N84766,
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ASN Wikibase Occurrence # 39468
 
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Date:Saturday 7 November 1992
Time:17:30 LT
Type:Druine Turbulent
Owner/operator:Mcrorey, Loelan J.
Registration: N84766
MSN: RWS-2
Total airframe hrs:5 hours
Engine model:Volkswagen
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Adelanto, CA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT WAS DEPARTING A DRY LAKE BED ON A LOCAL FLIGHT. GROUND WITNESSES REPORTED THAT UPON REACHING BETWEEN 50 AND 60 FEET ABOVE THE GROUND THE ENGINE SUSTAINED A TOTAL LOSS OF POWER. INSTEAD OF LANDING STRAIGHT AHEAD IN THE OPEN AREA THE PILOT ELECTED TO EXECUTE A RIGHT TURN. THE AIRCRAFT STALLED DURING THE TURN AND PLUNGED NOSE DOWN INTO THE GROUND. THE ENGINE EXAMINATION DISCLOSED NO EVIDENCE OF ANY INTERNAL CATASTROPHIC FAILURES. THE AIRFRAME FUEL SYSTEM AND THE ENGINE ACCESSORIES WERE DESTROYED. THE AIRCRAFT'S MAINTENANCE RECORDS DISCLOSED THAT THE PILOT/OWNER/BUILDER HAD NOT PERFORMED ANY CONDITION INSPECTIONS AS REQUIRED BY CURRENT FEDERAL AIR REGULATIONS SINCE IT RECEIVED ITS SPECIAL EXPERIMENTAL AIRWORTHINESS CERTIFICATE ON OCT 22, 1986. THE PILOT'S RECORDS WERE NOT RECOVERED. ACCORDING TO THE FAA, THE PILOT RECEIVED HIS LAST SECOND CLASS MEDICAL CERTIFICATE ON DECEMBER 27, 1990. HE INDICATED ON THE MEDICAL APPLICATION FORM THAT HE HAD ACCRUED 430 HOURS. THE AIRCRAFT LOG BOOK REVEALED THAT THE PILOT HAD FLOWN THE ACCIDENT AIRCRAFT FOR 5 HOURS AND 12 MINUTES.

Probable Cause: THE PILOT'S IMPROPER EMERGENCY DECISION TO ATTEMPT TO RETURN TO THE DEPARTURE AREA. CONTRIBUTING TO THIS ACCIDENT WAS THE UNDETERMINED LOSS OF POWER, INADEQUATE ALTITUDE, AND FAILURE TO MAINTAIN THE AIRSPEED.

Accident investigation:
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Investigating agency: NTSB
Report number: LAX93LA032
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX93LA032

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Apr-2024 16:55 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report]

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