Accident Beechcraft 58 Baron N770X,
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ASN Wikibase Occurrence # 39717
 
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Date:Friday 20 April 1990
Time:01:11
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Air Exchange Inc
Registration: N770X
MSN: TH-23
Engine model:CONTINENTAL IO-520-C
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Dallas, TX -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Unknown
Departure airport:(DAL)
Destination airport:Abilene, TX (ABI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PLT STARTED TO TAKE OFF ON RWY 13R, BUT ABORTED, TAXIED OFF THE RWY & WENT TO THE ENG RUN-UP AREA. ABT 2 MIN LATER, HE ANNOUNCED AGAIN THAT HE WAS READY TO DEPART & WAS CLRD TO TAKE OFF. DURING THE INITIAL CLIMB AFTER LIFT-OFF, THE PLT STATED THAT HE NEEDED TO RETURN FOR LNDG. HE WAS CLRD TO LND ON ANY RWY & HE DECIDED TO LND ON RWY 31L. WITNESSES OBSERVED THE ACFT IN A SHARP DSCNDG TURN FROM ABT 800' AGL AS IT WAS MANEUVERED BACK TOWARD THE RWY. HOWEVER, THE DSCNT RATE INCREASED, THEN THE ACFT CRASHED ABT 1000' SHORT OF THE RWY. DURING IMPACT, IT HIT A LAMP POLE & POWER LINE, THEN CAME TO REST & BURNED. THE FUEL BOOST PUMP SWITCHES WERE FND IN THE 'HIGH' BOOST POSITIONS & THE RGT PROP CONTROL WAS FND IN THE FEATHER POSITION. THE FLT MANUAL RCMDD THAT THE BOOST PUMPS BE IN THE 'LOW' POSITION FOR TAKEOFFS & LNDGS. A TEST OF THE USE OF THE HIGH BOOST POSITION IN A SIMILAR ACFT RESULTED IN A ROUGH RUNNING ENG & ENG STOPPAGE. A WITNESS TO THE ACDNT RPRTD THAT HE HEARD THE ENG SPUTTERING & MISFIRING BEFORE THE ACFT CRASHED. CAUSE: THE PILOT'S IMPROPER USE OF THE FUEL BOOST PUMPS FOR TAKE, AND HIS FAILURE TO MAINTAIN AIRSPEED ABOVE THE MINIMUM SINGLE ENGINE CONTROL SPEED (VMC), WHICH RESULTED IN A LOSS OF AIRCRAFT CONTROL.

Sources:

NTSB: https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X22922

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]

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