Accident Rand Robinson KR-2 N9667N,
ASN logo
ASN Wikibase Occurrence # 41188
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 30 June 1992
Time:18:15 LT
Type:Silhouette image of generic KR2 model; specific model in this crash may look slightly different    
Rand Robinson KR-2
Owner/operator:Lee, Eugene D.
Registration: N9667N
MSN: 1MD1
Engine model:Volkswagen 2100R-D
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Homestead, FL -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(X51)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
BEFORE THE ACCIDENT FLT, THE PLT WAS SEEN WORKING ON THE ENG ASSY. THE FLT DEPARTED & SHORTLY AFTER TAKEOFF, WITNESSES HEARD THE ENG RUNNING ROUGH, & OBSERVED THE PLT BANK THE ACFT TO RETURN TO THE ARPT. THE ACFT STALLED & IMPACTED THE GROUND NOSE LOW. ACCORDING TO A DETECTIVE WHO EXAMINED THE ACFT AT THE ACCIDENT SITE, THERE WAS NO ODOR OF FUEL. EXAMINATION OF THE FUEL TANK, GASCOLATOR (BOTH IMPACT DAMAGED) & CARBURETOR REVEALED NO EVIDENCE OF FUEL. THE CARBURETOR WAS FOUND DISCONNECTED FROM THE FLEXIBLE HOSE ATTACHED TO THE INTAKE MANIFOLD. THE FUEL SELECTOR WAS IN THE ON POSITION. THE PROPELLER WAS ROTATED & 3 OF THE 4 CYLINDERS PRODUCED COMPRESSION. THE LEFT REAR CYLINDER DID NOT DUE TO A STICKING EXHAUST VALVE. ADDITIONALLY, THE RT FWD TOP IGNITION LEAD WAS DISCONNECTED. THE THREADS ON THE LEAD & PLUG WERE NOT DAMAGED. ALSO, SEVERAL OF THE IGNITION LEADS WERE FINGER TIGHT ON THEIR RESPECTIVE SPARK PLUGS.

Probable Cause: INADVERTENT STALL BY THE PILOT WHILE ATTEMPTING TO RETURN TO THE AIRPORT FOLLOWING LOSS OF ENGINE POWER. CONTRIBUTING TO THE ACCIDENT WAS THE LOSS OF POWER DUE TO A STICKING EXHAUST VALVE, AND FAILURE OF THE PILOT TO ASSURE ALL IGNITION LEADS WERE CONNECTED AND TIGHTENED BEFORE THE FLIGHT.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA92LA144
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB MIA92LA144

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
11-Apr-2024 06:06 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org