ASN Wikibase Occurrence # 41201
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Date: | Saturday 27 November 1999 |
Time: | 15:55 LT |
Type: | de Havilland Canada DHC-2 Beaver |
Owner/operator: | William S. Warren |
Registration: | N666XT |
MSN: | 826 |
Total airframe hrs: | 15540 hours |
Engine model: | P&W R-985-AN39A |
Fatalities: | Fatalities: 4 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Washougal, WA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Witnesses reported that following takeoff from a river, the aircraft climbed to approximately 100 to 400 feet above the water, then initiated a left turn of approximately 45 degrees bank. The majority of the witnesses reported that after the aircraft had turned about 180 degrees, its nose abruptly dropped and it impacted the water. Witnesses did not report observing any evidence of problems with the aircraft before impact, and did not report hearing any abnormal engine sounds or sudden changes in engine pitch. Upon water impact, the aircraft went inverted and its cabin submerged. Efforts by witnesses to gain entry to the aircraft cabin to render assistance were unsuccessful due to aircraft damage. Rescue divers found all occupants deceased in the aircraft upon arrival, but were able to remove the two rear-seat victims without removing any passenger restraints. Autopsies disclosed that all four aircraft occupants had drowned. Investigators did not find any evidence of pre-impact aircraft or engine malfunctions during post-accident examinations of the wreckage, but did find that a cabin entry door was jammed shut due to impact damage, and that the range of travel of both pilot doors was restricted by damaged aircraft components.
Probable Cause: The pilot's failure to ensure attainment of adequate airspeed prior to initiating a steep turn at low altitude, resulting in an accelerated stall. A factor contributing to the occurrence of the accident was the aircraft's low altitude. Factors contributing to the severity of the accident included a water impact, and jammed/restricted doors due to impact damage resulting in degraded aircraft evacuation capability.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA00FA023 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB SEA00FA023
History of this aircraft
Other occurrences involving this aircraft
11 June 1987 |
N98EL |
Alaska Enchanted Lake Lodge |
0 |
King Salmon, AK |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
14-Aug-2011 08:03 |
TB |
Updated [Time, Cn, Phase, Departure airport, Source] |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:46 |
ASN Update Bot |
Updated [Cn, Operator, Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 16:50 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report] |
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