ASN Wikibase Occurrence # 42440
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Date: | Wednesday 25 September 1991 |
Time: | 13:30 |
Type: | Boland/Poe TSUNAMI |
Owner/operator: | Private |
Registration: | NX39JR |
MSN: | 001 |
Total airframe hrs: | 200 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Pierre, SD -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Casper, WY (CPR) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACCIDENT AIRPLANE WAS OBSERVED TO SUDDENLY ROLL INVERTED DURING FINAL APPROACH AND DESCEND INTO THE GROUND. INVESTIGATION OF THE WRECKAGE SHOWED A BENDING OVERLOAD FAILURE OF THE EXTERNAL THREADED STEM TYPE ROD END BEARING ATTACHED TO THE PISTON OF EACH WING FLAP HYDRAULIC ACTUATOR. THE EXPERIMENTAL RACING AIRPLANE WAS ORIGINALLY BUILT AND FLOWN WITHOUT WING FLAPS. THE WING FLAPS WERE ADDED BY THE PILOT/OPERATOR AT A LATER DATE. CAUSE: A BENDING OVERLOAD FAILURE OF THE WING FLAP CONTROL RODS AND REMEDIAL ACTION BY THE PILOT WAS NOT POSSIBLE. FACTORS IN THE ACCIDENT ARE THE INADEQUATE DESIGN OF THE WING FLAP SYSTEM BY THE PILOT/OPERATOR MANUFACTURER AND HIS LACK OF TOTAL EXPERIENCE IN TYPE OF AIRCRAFT.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X18049 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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