ASN Wikibase Occurrence # 42741
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Date: | Saturday 26 November 1983 |
Time: | 12:20 |
Type: | Beechcraft V35B Bonanza |
Owner/operator: | private |
Registration: | N9002Q |
MSN: | D-9166 |
Total airframe hrs: | 1170 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Cairo, IL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT DOVE INTO THE GROUND NOSE FIRST FROM A 90 DEGREE BANK SHORTLY AFTER TAKEOFF. THE ACFT WAS OBSERVED BY WITNESSESTO TAKE OFF SLOWLY 'WITH ABOUT 1/2 POWER' BEING USED. THE CLIMB WAS SLOW AND AT 300-400 FT THE ACFT TURNED LEFT WITH THELANDING GEAR STILL DOWN. WITNESSES NEAR THE ACCIDENT SITE HEARD THE ENGINE SPUTTER. WHEN THE ENGINE SPUTTERED A 2ND TIMETHE ACFT TURNED LEFT WITH SOME LOSS OF ALTITUDE. WHILE IN THIS TURN 'THE WING DIPPED DOWN SUDDENLY' TO ABOUT A 90 DEGREEBANK ANGLE. THE ACFT DOVE TO THE GROUND AND EXPLODED. THE INVESTIGATION REVEALED THE FUEL SELECTOR NEAR THE RIGHT FUEL TANK POSITION. THE VALVE WAS OPEN ONLY PART WAY AND DURING TESTING THIS INTERFERED WITH FUEL FLOW AND AFFECTED THE ABILITY OF THE FUEL PUMP TO SUPPRESS VAPOR FORMATION. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X45010 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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