ASN Wikibase Occurrence # 43100
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Date: | Friday 11 August 2000 |
Time: | 19:00 |
Type: | Murphy SR2500 Super Rebel |
Owner/operator: | Private |
Registration: | N24VW |
MSN: | 024 |
Total airframe hrs: | 48 hours |
Engine model: | Continental IO-470-D |
Fatalities: | Fatalities: 2 / Occupants: 4 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bakersfield, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an emergency landing the left wing of the airplane struck an irrigation standpipe, and the airplane was destroyed in a post impact fire. The pilot reduced the power to descend and circle to land at a dirt airstrip. When he advanced the throttle to arrest the airplane's descent there was no corresponding power increase. He conducted the emergency procedures, but was unable to restart the engine. He overflew the airstrip and attempted an emergency landing in a cornfield. Review of the airplane's power plant logbook revealed that an overhauled engine had been installed on the experimental airplane in March 1999. The last entry was December 8, 1999, when the engine was test ran, and the fuel injection system was adjusted according to manufacturer's specifications. No further entries were found in the airframe or power plant logbooks. During the engine examination the throttle valve was found jammed in the closed position. Investigators also found the idle speed stop screw backed off from the throttle shaft arm about 1/8 inch. No further mechanical anomalies were noted.
Probable Cause: Adjustment by other maintenance personnel of the idle speed stop screw. The idle speed stop screw was backed off from the throttle shaft arm, not allowing the butterfly valve to operate properly, which resulted in the butterfly valve remaining closed during a power input via the throttle control linkage during the approach to landing phase.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00LA293 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X21769&key=1 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 19:04 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
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