ASN Wikibase Occurrence # 43276
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 19 June 1993 |
Time: | 05:10 LT |
Type: | Hughes 500D (369D) |
Owner/operator: | Skydance Operations, Inc. |
Registration: | N277SP |
MSN: | 290461D |
Year of manufacture: | 1979 |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Half Moon Bay, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed his residence in the southern California area at 1030 on June 18th and flew commercially to Reno, Nevada. The pilot was to pick up the helicopter and ferry it to a movie filming location at the accident site, where it was to be used as a camera platform. The pilot arrived in Reno at 1300 hours and was informed that the helicopter was not at the airport and ground transportation would be sent to take him to the helicopter. The pilot waited in the airport terminal until 1630 hours for ground transportation to arrive. At 1745 hours the pilot departed in the accident helicopter and arrived at the filming site about 1850 hours. The actual filming started just after midnight on saturday morning and concluded at 0300 hours that morning. About 0410 hours the pilot was maneuvering the helicopter to depart the area when it collided with a power cable attached to an illuminated bank of high intensity lights mounted on top of a 125 foot tall telescoping tower used during the filming. The impact occurred on the same side of the tower as the two million candle power lights. The accident occurred about 17 hours after the pilot had departed his residence.
Probable Cause: the pilots failure to maintain an adequate clearance from the light tower and associated electrical power cables. Factors in the accident were; 1) pilot fatigue due to an excessively long duty day, and 2) glare from the lights which affected the pilot's ability to clearly see the obsturctions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX93LA261 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB LAX93LA261
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 13:09 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation