Accident Beechcraft A90 King Air N518DM,
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ASN Wikibase Occurrence # 43374
 
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Date:Saturday 31 July 1999
Time:08:25 LT
Type:Silhouette image of generic BE9L model; specific model in this crash may look slightly different    
Beechcraft A90 King Air
Owner/operator:Parahawks Skydiving Center
Registration: N518DM
MSN: LJ-251
Year of manufacture:1967
Total airframe hrs:8986 hours
Engine model:P&W PT6A-20
Fatalities:Fatalities: 10 / Occupants: 10
Aircraft damage: Destroyed
Category:Accident
Location:Marine City, MI -   United States of America
Phase: Initial climb
Nature:Parachuting
Departure airport:(76G)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane impacted the terrain approximately 2,065 feet south of the departure end of runway 22. Damage to the cockpit section of the wreckage indicated a nose down crush angle of approximately 80 degrees. The wreckage path was on a 208 degree heading, and the distance from the initial impact to the location of the empennage was about 142 feet. The cockpit and cabin were destroyed by post impact fire. Examination of the engines and propellers revealed no preexisting failures or conditions that would have prevented normal operation. The engines exhibited indications of rotation, and the witness marks on both sets of propellers were consistent with the propellers operating in the governing range at impact. Control continuity was established from the right aileron, elevator, and rudder. Witnesses reported the airplane seem to be operating normally during taxi and takeoff, but that it entered a steep left bank after clearing a 100 foot powerline located about 1,800 feet from the departure end of runway 22. After entering the steep left turn, the nose of the airplane dropped and the airplane impacted the ground. There was no evidence in the airplane's maintenance records of any annual maintenance inspection since August, 1997, although an airframe and powerplant mechanic reported that he had completed an inspection on June 30, 1999. There was no record in the airplane's mainteance records of compliance with five airworthiness directives applicable to the airplane.

Probable Cause: The pilot's failure to maintain adequate airspeed, which resulted in a stall, inflight loss of contol, and collision with the ground.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI99MA269
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB CHI99MA269

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
14-Dec-2017 08:42 ASN Update Bot Updated [Nature, Departure airport, Source, Narrative]
17-Nov-2022 08:10 Ron Averes Updated [Aircraft type, Narrative]
07-Apr-2024 18:58 ASN Update Bot Updated [Time, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report]

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