ASN Wikibase Occurrence # 43374
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Date: | Saturday 31 July 1999 |
Time: | 08:25 LT |
Type: | Beechcraft A90 King Air |
Owner/operator: | Parahawks Skydiving Center |
Registration: | N518DM |
MSN: | LJ-251 |
Year of manufacture: | 1967 |
Total airframe hrs: | 8986 hours |
Engine model: | P&W PT6A-20 |
Fatalities: | Fatalities: 10 / Occupants: 10 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Marine City, MI -
United States of America
|
Phase: | Initial climb |
Nature: | Parachuting |
Departure airport: | (76G) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted the terrain approximately 2,065 feet south of the departure end of runway 22. Damage to the cockpit section of the wreckage indicated a nose down crush angle of approximately 80 degrees. The wreckage path was on a 208 degree heading, and the distance from the initial impact to the location of the empennage was about 142 feet. The cockpit and cabin were destroyed by post impact fire. Examination of the engines and propellers revealed no preexisting failures or conditions that would have prevented normal operation. The engines exhibited indications of rotation, and the witness marks on both sets of propellers were consistent with the propellers operating in the governing range at impact. Control continuity was established from the right aileron, elevator, and rudder. Witnesses reported the airplane seem to be operating normally during taxi and takeoff, but that it entered a steep left bank after clearing a 100 foot powerline located about 1,800 feet from the departure end of runway 22. After entering the steep left turn, the nose of the airplane dropped and the airplane impacted the ground. There was no evidence in the airplane's maintenance records of any annual maintenance inspection since August, 1997, although an airframe and powerplant mechanic reported that he had completed an inspection on June 30, 1999. There was no record in the airplane's mainteance records of compliance with five airworthiness directives applicable to the airplane.
Probable Cause: The pilot's failure to maintain adequate airspeed, which resulted in a stall, inflight loss of contol, and collision with the ground.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI99MA269 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI99MA269
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 08:42 |
ASN Update Bot |
Updated [Nature, Departure airport, Source, Narrative] |
17-Nov-2022 08:10 |
Ron Averes |
Updated [Aircraft type, Narrative] |
07-Apr-2024 18:58 |
ASN Update Bot |
Updated [Time, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
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