ASN Wikibase Occurrence # 43851
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Date: | Thursday 8 March 2007 |
Time: | 15:02 |
Type: | Aérospatiale AS 350BA |
Owner/operator: | Heli-USA Airways, Inc. |
Registration: | N354NT |
MSN: | 1168 |
Year of manufacture: | 1979 |
Total airframe hrs: | 21706 hours |
Engine model: | Turbomeca Arriel 1B |
Fatalities: | Fatalities: 4 / Occupants: 7 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Princeville Airport, Kauai, HI -
United States of America
|
Phase: | Landing |
Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
Departure airport: | Princeville, HI (HI01) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter was returning from a sightseeing flight when the pilot contacted the dispatcher and announced, "I'm having hydraulic problems, and I'm probably going to have to do a run-on landing." The language he used to describe his situation changed from "hydraulic problem" to "hydraulic failure" as the flight proceeded. The pilot did not immediately land at the approach end of the runway; instead, he continued to the departure end, where the passenger terminal was located. The helicopter approached the mid-point of the runway, and as it neared the surface, the dispatcher heard the pilot state, "Okay we're done." Then, the sound of the rotor changed pitch and the helicopter impacted the ground. Postaccident examination of the helicopter revealed that the left lateral flight control servo became disconnected in flight at the transmission. Further examination revealed that the lower clevis of the left lateral servo was still attached to the transmission case, but was no longer attached to the servo. The threads on the clevis, as well as the threads on the inner diameter of the servo, appeared undamaged. The jam nut, lock nut washer, and safety wire were still attached to the clevis threads and rotated freely. The lock washer was severely worn and the locking tang was missing. Metallurgical testing and torque testing of the accident servos revealed that the jam nut, washer, and piston rod were able to easily rotate off of the clevis if no torque was applied and with the locking tang missing. Under normal loads, the main hydraulic flight control servos experience slight twisting that could contribute to the servo rotating off the clevis bolt (without an intact and functioning locking washer installed). Therefore, the investigation revealed that the servo attachment nut was not torqued during maintenance about one month prior to the accident, and the lack of torque, coupled with the installation of a severely worn lock washer, allowed the servo to rotate off of the clevis during the accident flight, resulting in a complete disengagement of the servo from its mounting clevis on the transmission. Examination of the company maintenance program revealed that none of the mechanics at the helicopter's base had received factory training, and that the maintenance manuals they used were three revisions out of date. Mandatory quality control inspections of maintenance actions, as well as post-maintenance test flights prescribed in the General Operator's Manual and the manufacturer's maintenance manuals (that included the replacement of the flight control servo), were not performed.
(This report was modified on June 16, 2009)
Probable Cause: The failure of maintenance personnel to properly tighten (torque) the flight control servo lower attachment clevis, and reinstall a functioning lock washer, which resulted in a flight control disconnect and a complete loss of helicopter control. Contributing to the accident was the operator's failure to ensure its maintenance program was being executed in accordance with Federal regulations.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07MA073 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070321X00315&key=1 FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=N354NT Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
16-Jul-2014 14:24 |
Dr. John Smith |
Updated [Time, Cn, Location, Nature, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:33 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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