Accident Hiller UH-12A N8180H,
ASN logo
ASN Wikibase Occurrence # 43859
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 24 February 2007
Time:15:08
Type:Silhouette image of generic UH12 model; specific model in this crash may look slightly different    
Hiller UH-12A
Owner/operator:Private
Registration: N8180H
MSN: 180
Engine model:Franklin 6VS-335 SER
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Bethlehem, GA -   United States of America
Phase: Take off
Nature:Training
Departure airport:Bethlehem, GA (PVT)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot attempted a downwind departure at or about maximum gross weight in a very tight landing zone with high obstacles, forcing the pilot to use rotor energy to gain altitude which would have slowed rotor RPM below safe operating limits. With a tailwind the engine had insufficient power for the helicopter to reach transitional lift. Once the pilot determined that he could not regain rotor speed, he would have selected an area in the woods to try and descend. Rotor RPM would have continued to decay and the pilot would have initiated an Auto-Rotation. The pilot closed the throttle as noted by the crushed throttle linkage. The tail-rotor descended into the trees as evidenced by impact marks to the leading edge of the tail-rotor blades. The engine was still developing power to the rotor system as observed in the twisting of the tail-rotor drive shaft aft of the tail-rotor universal joint. The helicopter descended through the trees vertically and nosed down when the main rotor blades exited the helicopter. The metal strip on the main rotor blades contacted the tail boom at the rear universal joint of the tail rotor drive shaft. The helicopter impacted the ground. The transmission and rotor system crushed the flight deck. Examination of the helicopter found no preimpact mechanical failure or malfunctions that would have prevented the helicopter from operating properly.
Probable Cause: The pilot's failure to maintain adequate rotor rpm, which resulted in an attempted autorotation and in-flight collision with trees. Contributing to the severity of the accident was the pilot exceeding the helicopters takeoff capability.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL07LA045
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070226X00225&key=1

History of this aircraft

Other occurrences involving this aircraft
16 September 1995 N8180H Private 0 Bonners Ferry, ID sub

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Dec-2017 18:30 ASN Update Bot Updated [Operator, Other fatalities, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org