ASN Wikibase Occurrence # 43943
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Date: | Monday 20 November 2006 |
Time: | 17:25 |
Type: | Piper PA-28-235 |
Owner/operator: | Private |
Registration: | N8990W |
MSN: | 28-10570 |
Year of manufacture: | 1964 |
Total airframe hrs: | 4457 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Wellington, IL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Peru, IL (VYS) |
Destination airport: | Indianapolis, IN (HFY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was destroyed during an in-flight collision with terrain during night visual meteorological conditions. The pilot contacted air traffic control (ATC) after takeoff and requested visual flight rules (VFR) flight following. ATC radar data indicated that the flight climbed to 5,500 feet mean sea level (msl) and proceeded on-course toward the intended destination. About 30 minutes into the flight, ATC informed the accident airplane of traffic in his vicinity. The other airplane was approximately 3 miles ahead of his position, northeast bound at 5,000 feet msl at that time. The accident pilot reported he did not have the traffic in sight. About 2 minutes later, ATC informed the accident pilot that the traffic was about 1-1/2 miles off his right wing. The pilot was also instructed to contact another ATC facility. The accident pilot did not respond to either transmission. The ATC radar track data suggested that the airplane subsequently entered a descending left turn, from a southeast course to a southwest course. The airplane appeared to level off at 4,900 feet msl momentarily, before it entered a descending right turn. The final radar data point was at 4,000 feet msl, which was the floor of radar coverage in the area. The airplane appeared to be in a right turn, passing through a northwest course at that time. The accident site was located approximately 1/2 mile east of the final radar data point. The accident site was located in a sparsely populated, rural agricultural area. The wreckage distribution was consistent with a low-level separation of the horizontal stabilator prior to impact. The examination also revealed that the right aft wing spars were bent upward and fractured at the wing-to-fuselage splice joint. All fracture surfaces were consistent with tensile overload failures. Stabilator and rudder control continuity was confirmed from the control surface to the aft cabin area. The post accident airframe and engine examination did not reveal any anomalies associated with an in-flight malfunction.
Probable Cause: Spatial disorientation experienced by the pilot while attempting to visually locate traffic during cruise flight, which resulted in a loss of aircraft control. Contributing factors were the inadvertent overload failure of the wing spar and stabilator, and the night lighting conditions.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20061127X01714&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
05-Dec-2017 09:28 |
ASN Update Bot |
Updated [Other fatalities, Source, Narrative] |
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