Accident Beechcraft A36 Bonanza N16JR,
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ASN Wikibase Occurrence # 44181
 
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Date:Monday 13 March 2006
Time:09:43
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Private
Registration: N16JR
MSN: E433
Total airframe hrs:3510 hours
Engine model:Teledyne Continental IO-520-BA
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Santa Monica, CA -   United States of America
Phase: Take off
Nature:Private
Departure airport:Santa Monica, CA (SMO)
Destination airport:San Diego, CA (SDM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The engine lost power during the takeoff-initial climb and the pilot ditched the airplane in the ocean. Examination showed that the number 2 connecting rod fractured from the crankshaft. Metallurgical examination of the connecting rod, and associated bolts, nuts, and bearings, showed that following the first nut and bolt separation, the overall separation was not instantaneous. After the first nut unthreaded from its respective bolt, subsequent increased loads on the opposite bolt then stripped the threads of the other nut that had partially unthreaded from its bolt. Furthermore, there was no evidence of cotter pin installation. In general, a properly torqued nut and connecting rod bolt will not loosen under normal operational conditions. The engine underwent a field overhaul 735.31 hours prior to the accident. At 233.59 hours prior to the accident, the cylinders were removed for a blow by condition during an annual inspection; however, the aviation maintenance technician who performed this work stated that he did not remove the connecting rods from the crankshaft. Review of the autopsy results and impact damage to the wreckage indicated that the occupants' use of shoulder harnesses would have significantly increased their chances of survival.
Probable Cause: The failure of an aviation maintenance technician to properly torque and cotter pin the number 2 connecting rod bolts at their attach point to the crankshaft, which resulted in the separation of the connecting rod in flight, and complete power loss.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX06FA129
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20060317X00321&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
05-Dec-2017 09:05 ASN Update Bot Updated [Operator, Other fatalities, Source, Narrative]

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